Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
16/5/2019 |
OCC1698 |
Lilydale Aerodrome |
VIC |
Jabiru |
J160 |
Jabiru |
2200 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft had been assessed as in airworthy condition. The...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft had been assessed as in airworthy condition. The front nose wheel was inspected prior to start up and nothing unusual was noticed. The aircraft was flown previously by a student, doing touch and go’s, and hadn’t been through any hard landings. After taxiing to southern end of the field and after TEMPFISCH checks/Run Up checks, the plane was taxied towards the beginning of the runway where the nose oleo leg failed without any prior symptoms. . Estimated speed at impact was a walking pace so no injuries were sustained. The propeller had hit the ground and had come to a stop in a diagonal position no longer touching the ground. The aircraft systems were shut off including the fuel cut off valve and the aircraft was evacuated.
It was found that the lower nose bungee attach fitting bolt was missing, either failed and fell out or the nut had detached and the bolt worked its way out. |
15/5/2019 |
OCC1699 |
Bankstown Aerodrome |
NSW |
Aeroprakt |
A22LS Foxbat |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The instructor was conducting a circuit emergency lesson for ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The instructor was conducting a circuit emergency lesson for aborted take-off practice. An aborted take-off was carried out which overheated the brakes once the ops were complete. A request clearance to vacate the RWY was made to ATC and the aircraft was advised to hold short of the crossing RWY. The aircraft was unable to come to a stop before the nose crossed the runway holding point due to the overheated brakes reducing braking effectiveness even with full brakes applied. Braking capacity was exceeded due to overheat. There was not enough time allowed to cool down to be effective prior to the incident. |
15/5/2019 |
OCC1735 |
Jandakot Aerodrome |
WA |
Evektor |
SportStar Plus |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was cleared for take-off from RWY 06L for a Frem...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was cleared for take-off from RWY 06L for a Fremantle departure, the pilot applied full power and started the ground roll. During the take off roll, the pilot heard a broken transmission, in which they recognised their call sign but not the complete message. The pilot continued to focus on the departure instruments and establishing a positive climb while maintaining a lookout on the circuit area. At about 500 AGL, as the pilot initiated left climbing turn into the crosswind and made a call to Jandakot tower, requesting a repeat of the last message. ATC advised on traffic and requested to widen out. The pilot sighted the traffic on what appeared to be the downwind leg for RWY 06L at a higher altitude and advised ATC accordingly. This was followed by an immediate instruction to underfly another aircraft. The pilot levelled off at about 800ft AMSL and proceeded on track for Murdoch University. Once clear of other traffic, the pilot re-established climb to 1000 AMSL. |
14/5/2019 |
OCC1719 |
Wangaratta |
VIC |
Aeropro |
3K Eurofox |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The muffler baffles were found to be disintegrating o...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The muffler baffles were found to be disintegrating on the aircraft. New baffles have been fitted. The manufacturer has been notified of the products TTIS. |
12/5/2019 |
OCC1682 |
Bunbury Aerodrome |
WA |
Tecnam |
P2002 Sierra |
Rotax |
912 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: A student on their second solo was conducting circuits with t...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: A student on their second solo was conducting circuits with the instructor was observing. On the fourth circuit, during the take-off, the instructor noted that the aircraft veered sharply to the left while still on the ground before it became airborne. The student appeared to attempt to clear the trees however the left wing dropped as a result of clipping a fence post and landed in the trees, facing back towards the runway.
A review of the accident was conducted by the flight school and RAAus.
The supervising instructor has determined through debrief that the student pilot rushed the take off on this touch and go and disregarded the school procedure to reject take offs if not fully satisfied with control. Subsequent remedial training has been undertaken and the pilot is continuing training towards their certificate. |
12/5/2019 |
OCC1686 |
Lilydale Aerodrome |
VIC |
Jabiru |
J160C |
Jabiru |
2200 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The student had successfully completed one circuit and landin...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The student had successfully completed one circuit and landing with one stage of flap, they had done so without any need for the instructor to come on the controls. The second landing (a touch and go) was flapless, the student had landed a little long. The grass RWY surface was a little rough and as the aircraft exceeded 60 knots, the student hadn’t rotated. Initially the instructor thought the student may have delayed rotation due to it being a flapless take-off and the instructor was concerned that the nose leg was being pounded. The instructor reached for the flap control and asked if the student required flap, the student responded by closing the throttle and saying that there was no aileron control. The instructor checked the control yolk which came away in their hand. The instructor aborted the take-off and rolled through the remaining RWY and taxied to the hangar.
For defect response see Jabiru Service Bulletin JSB 042-1 |
11/5/2019 |
OCC1681 |
Archerfield Aerodrome |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912IS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: As the aircraft entered the runway the brakes were observed t...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: As the aircraft entered the runway the brakes were observed to have failed. Brake fluid was observed leaking from the left side and the brake pad was also observed to be missing.
Brake pad worn beyond limits |
8/5/2019 |
OCC1685 |
Jacobs Well Aerodrome |
QLD |
Aeroprakt |
Foxbat A22LS |
Rotax |
912 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Upon completion of a flight and taxiing the aircraft to the p...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Upon completion of a flight and taxiing the aircraft to the parking area the nose leg partially collapsed. This occurred at a speed of approx. 5km per hour whilst the aircraft was under gentle braking and a meter or so from its intended destination. This occurred due to failure of a mounting bracket that attaches to the nose wheel fork and allows the bracket to pivot in a scissor action. |
8/5/2019 |
OCC1678 |
Bankstown Aerodrome |
NSW |
Tecnam |
P2008 |
Rotax |
912ULS2-01 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The instructor misinterpreted the ATC clearance to line up to...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The instructor misinterpreted the ATC clearance to line up to include a clearance to take off. Contributing factors included expectation bias by the Instructor based on previous clearances for earlier flights on the same day along with fatigue and lapse in concentration. Training practices and revision of clearance phraseology have been reviewed and modified with the instructor and CFI of the school. |
3/5/2019 |
OCC1675 |
Caboolture Airport |
QLD |
Texan |
Top Class 550 |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: While moving the aircraft within the hangar, the nose...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: While moving the aircraft within the hangar, the nose wheel rotated 90 degrees. Upon investigation it was found that the steering plate at the top of the nose strut has corroded and broken completely around the mounting nut. Advisory Notice ADN/Flysynthesis/1 issued 10 May 2019. |
1/5/2019 |
OCC1673 |
Lilydale Aerodrome |
VIC |
Jabiru |
J160D |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: When taxiing south towards RWY 36L at low speed the right han...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: When taxiing south towards RWY 36L at low speed the right hand main landing gear collapsed and the nose of the aircraft veered towards the right.
Bolt failure pictures reveal tensile fatigue failure, causal factors could be over torqued bolt, hard landing or overloaded aircraft ( operated above MTOW). Impossible to rule out a manufacturing defect in the metallurgy of the bolt however the most likely cause may have been a hard landing at some stage in the previous 280 hours since this bolt was installed. |
1/5/2019 |
OCC1683 |
Lilydale Airport |
VIC |
Jabiru |
J-160-D |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The right hand main landing gear leg inboard attach bolt was ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The right hand main landing gear leg inboard attach bolt was broken. |
30/4/2019 |
OCC1671 |
Parkes Airport |
NSW |
Flight Design |
CTMC |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Carrying out touch and go circuits with a trainee pil...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Carrying out touch and go circuits with a trainee pilot, the instructor noticed a shimmy in the nose wheel on consecutive take-off runs. Checks after the flight confirmed an undesirable "slop" was present in the nose wheel and the aircraft was referred to a local aircraft maintenance organisation for further investigation.
Large cracks were discovered in two elements of the support structure for the nose-leg, and the aircraft was taken off-line pending repair or replacement of the part. |
30/4/2019 |
OCC1670 |
Charleville |
QLD |
I C P |
Savannah VG |
Rotax |
912 U L S |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Engine began to run rough at full throttle after initiating a...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Engine began to run rough at full throttle after initiating a climb. Reduction in throttle and application of boost pump seemed to stop rough running. Pilot performed a precautionary landing at a private airstrip after contacting Brisbane Centre and declaring a partial engine failure.
Following a normal landing, ground running indicated no further issue. Cowls were removed and engine inspected visually with no apparent damage. Fuel was drained at header tank to test for presence of water, however none was found.
Investigations with the authorised maintainer and the pilot have indicated no pre existing mechanical issues were likely to have contributed to the engine issues experienced by the pilot which required a precautionary landing to be undertaken. A review of environmental conditions and the operation of the aircraft in an extended descent to avoid cloud en route were significant contributing factors to a partial carburettor icing condition. The pilot has since conducted a full drain of the fuel system and tested the aircraft without any further engine issues.
This incident also revealed a number of non contributing elements worthy of awareness for all pilots including adopting an accurate flight notification process and ensuring BFR compliance has been notified and recorded by RAAus when completed by an alternate means. |
30/4/2019 |
OCC1672 |
Clifton Aerodrome |
QLD |
Jabiru |
J160 C |
Jabiru |
2200 A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst conducting circuit training on RWY06, the Jabiru was o...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst conducting circuit training on RWY06, the Jabiru was on climb out and turning onto crosswind at 2100ft (600ft AGL) when a Cessna 170 aircraft announced they were on base for RWY24 at 2200 feet (700ft AGL), their broadcast did not indicate the airfield. The Jabiru pilot requested they identify the airfield and they responded with "Clifton" to which the Jabiru advised that they were on climb out. The pilot of the Cessna 170 subsequently dived under the Jabiru 24-4498. Neither aircraft had seen each other at this point. The pilot of the Jabiru now observed the Cessna on left downwind for RWY 06 and further radio communication ensured the Cessna pilot complied with a circuit join for a right downwind to 06.
During a later discussion, the pilot of the Cessna said they were on the wrong frequency until Brisbane Centre had informed them of the incorrect frequency when they were established in the circuit. |