Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
18/11/2019 |
OCC1866 |
Barwon Heads Aerodrome |
VIC |
Brumby |
LSA R610 |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: An RAAus registered aircraft that was uncontactable on radio ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: An RAAus registered aircraft that was uncontactable on radio via Barwon Heads CTAF and Melbourne Centre when it flew near to skydivers in a drop zone.
The pilot was interviewed by RAAus and it was determined some confusion about the correct frequencies and procedures existed. The pilot completed a ground review with a RAAus Pilot Examiner and has now adopted improved procedures to ensure adequate separation from parachute aircraft and parachutists.
RAAus pilots are reminded to ensure they reference appropriate charts for the proposed flight area to confirm radio frequencies and comply with procedures at uncontrolled aerodrome as per Civil Aviation regulation (CAR) 166 and guidance material provided in the latest version of Civil Aviation Advisory Publication (CAAP) 166. |
17/11/2019 |
OCC1874 |
Miles |
QLD |
Rand Kar |
X Air |
Jabiru |
2200 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Climbing out, normally get 3000 RPM, got to 300', got a rev d...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Climbing out, normally get 3000 RPM, got to 300', got a rev drop, confirmed with the tcho 2800 rpm, over trees away from the strip, turned around to return to the strip, got to gliding distance, back to idle, lots of vibration, applied a small amount of power to remove engine vibration, landed safely, no injury to people, no damage to aircraft.
Subsequent investigation revealed part of the side of the #4 piston had a piece missing, top ring damaged, area between 1 and 2 ring damaged. |
17/11/2019 |
OCC1868 |
Ayr Aerodrome |
QLD |
Jabiru |
J170C |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During dual flight training, on climb out after take-off from...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: During dual flight training, on climb out after take-off from Ayr aerodrome there was a loud thump noise with a sudden loss of power. The instructor immediately took over control and turned the aircraft towards the aerodrome hoping to make a landing on RWY 11. Despite having a tailwind at that point the glide was not progressing as well as expected, so the instructor repositioned the aircraft for an approach to an obstacle free headland between two recently harvested sugar cane blocks. The aircraft landed on the headland without any damage. |
16/11/2019 |
OCC1865 |
Renmark |
SA |
Evektor |
Sportstar |
Rotax |
912 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft made contact with power lines resulting in colli...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft made contact with power lines resulting in collision with terrain and serious injury to the pilot |
16/11/2019 |
OCC1864 |
Goulburn Aerodrome |
NSW |
Skyfox |
CA25N Gazelle |
Rotax |
912A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was returning to the airfield after a dual train...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was returning to the airfield after a dual training flight. During the cruise, the aircraft began vibrating abruptly and aggressively. The instructor immediately took back control and began to troubleshoot the issue. During this time, the engine RPM was fluctuating but more-or-less stable and in the vicinity of its normal cruise setting.
Troubleshooting confirmed that the issue was engine related, during which the instructor also confirmed the aircraft had either full power with no vibration, or low and decreasing power with considerable vibration. The instructor opted to maintain height and full power and continue tracking towards Goulburn and also commenced a standard forced landing drill, preparing the aircraft, cabin and student for any deterioration that would require such a landing.
During the flight back the situation deteriorated with power decreasing to idle with significant vibration and backfiring before spiking back to full power and repeating this pattern several times. As a result, the instructor declared a PAN PAN on the CTAF frequency (127.150) primarily to let other aircraft operating within the area know the situation and the intention of continuing towards the airport as a priority.
During the approach and descent, the engine at full power and the instructor planned to make a gradual descent towards RWY 22 at high speed and shut the engine down shortly before touchdown, trading airspeed for altitude as necessary. The aircraft landed uneventfully.
The aircraft was pushed back to the hangar, and inspection revealed that the left throttle control cable had snapped. |
12/11/2019 |
OCC1870 |
Wellcamp Aerodrome |
QLD |
Jabiru |
J-230D |
Jabiru |
Jabiru 3300A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot took off from the TWY instead of the RWY and did no...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot took off from the TWY instead of the RWY and did not realise the error until after take-off. This was due to the pilot being unfamiliar with the airport and the wide TWYs. |
10/11/2019 |
OCC1861 |
Heck Field Aerodrome |
QLD |
Aeroprakt |
A22LS Foxbat |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst conducting the pre-landing checks it was discovered th...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst conducting the pre-landing checks it was discovered that the brakes had no pressure. A touch and go landing was conducted to ascertain the feasibility of a full stop landing. Subsequently a successful full stop landing was conducted which resulted in nil damage to aircraft or injuries to occupants.
Hydraulic hose split allowing the brake fluid to drain from the system in flight. |
9/11/2019 |
OCC1860 |
Caboolture Aerodrome |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912ULS2-01 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Following a control upset in the landing flare which resulted...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Following a control upset in the landing flare which resulted in the aircraft bouncing, the pilot elected to conduct a missed approach. On the subsequent approach a successful flare and landing was conducted but the nose wheel of the aircraft collapsed during roll out with the resultant additional damage.
Post accident investigation by the authorised maintainer could not determine any pre existing defect in the nose leg and the failure was most likely the result of over stress during the initial landing attempt. A combination of control management, environmental conditions and camber of the runway intersection which can act like a "ramp" in stronger westerly conditions are the likely factors that contributed to the initial Loss of Control resulting in aircraft damage. |
6/11/2019 |
OCC1858 |
Warwick Aerodrome |
QLD |
Zlin Aviation |
Savage Cub |
Rotax |
912S |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was on final approach to the grass strip after o...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was on final approach to the grass strip after only one circuit, on correct speed and profile. Wind was light. CAVOK. At about 20ft height, a bang sounded, and the right rudder failed completely. It sat limply against the firewall. Because the rudder pedals are spring-loaded, this resulted in an unrecoverable full left rudder deflection. The airplane yawed and rolled sharply left, flying low over the bitumen runway. A brief burst of power to recover airflow and control over the rudder was to no avail, except briefly keeping the aircraft at about 20ft height. The rudder remained in a left hard-over and the aircraft kept yawing and rolling left.
The left wing then dropped completely and impacted the grass on the left of RWY 27, cartwheeling the aircraft onto its nose. This separated the three propeller blades as they dug into the dirt. The nose impact also stopped the engine. The fuselage was at right angles to the ground now, with the tail pointing skyward. The aircraft then continued cartwheeling onto its right wing, and the fuselage came back down, tearing off the undercarriage and bending and severely damaging the tail assembly. It came to rest close to the southern boundary fence of the aerodrome, laying on its right wing at 270 degrees to the original approach direction. PIC and PAX were able to exit the aircraft.
Manufacturer released safety alert No 11 on the 14/01/2020 for a mandatory rudder cable inspection before next flight. |
2/11/2019 |
OCC1859 |
Archerfield Aerodrome |
QLD |
Aeropro |
3K Eurofox |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The student pilot was conducting solo circuits when the wind ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The student pilot was conducting solo circuits when the wind picked up. They elected to complete the session but due to the prevailing conditions conducted a missed approach. The subsequent full stop landing was harder than normal and bounced a little but the aircraft landed safely and exited the runway stopping after the holding point. The student stated that the aircraft was stopped with the park brake on when a gust of wind flipped the aircraft onto its back.
An investigation of the flight planning and reported weather conditions was undertaken and found to be acceptable and the student had flown in similar observed and forecast conditions previously. Ground control management was also reviewed. The flight school is reviewing the time periods for supervised solo operation during the current volatile weather following this accident as part of its ongoing risk mitigation. |
1/11/2019 |
OCC1854 |
Bankstown Aerodrome |
NSW |
Aeroprakt |
A22LS Foxbat |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The nose wheel of the aircraft collapsed upon landing. The pi...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The nose wheel of the aircraft collapsed upon landing. The pilot went around, assessed the issue and landed safely.The report was investigated reviewing both operational and technical elements. Maintenance, airworthiness and other technical considerations were ruled out and the most likely identified primary cause was aircraft control management during landing.The flight school was contacted to request a review of the pilots training and performance which was completed.. |
1/11/2019 |
OCC1853 |
Bowen Aerodrome |
QLD |
ICP |
Savannah S |
Savannah |
SVG |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft is reported to have taken off and then landed th...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft is reported to have taken off and then landed the next day without making any radio calls. As the aircraft landed there was a local skydive aircraft with 5 people on board in the air ready to drop skydivers.
Further investigation revealed the pilot had flown into the CTAF without a working radio. The aerodrome has a radio carriage and use requirement.
The pilot is undertaking retraining with a RAAus CFI regarding these requirements. |
27/10/2019 |
OCC1851 |
Greenside ALA |
WA |
ICP |
Savannah VG |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The Trim tab was able to move freely up and down appr...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The Trim tab was able to move freely up and down approx. 10 - 12 mm. This caused the aircraft's elevator to be neutrally stable to marginally unstable if the control column was released during flight, and this effect was exacerbated due to light air turbulence.
Upon inspection the actuation / trim control system was found to be loose with rod ends indicating wear. The trim tab control bell crank was also loose and allowed some additional play of the trim tab. There was also some looseness of the trim tab piano hinge due to narrow gauge wire in the hinge.
Worn components, checking for wear and play in the controls systems is a requirement during the 100/ annual inspection. |
27/10/2019 |
OCC1863 |
Palmyra Airstrip |
QLD |
Tecnam |
P92 Eaglet |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Whilst completing a pre-flight inspection, the pilot ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Whilst completing a pre-flight inspection, the pilot detected movement in the LH elevator (up/down and fore/aft). An L2 was called and they determined that the movement was from within the elevator itself. The LH elevator was removed and it was found that the holes in the torque tube and the elevator had been drilled oversize. There is a single M8 bolt inside a 10mm OD bush holding the elevator halve to the torque tube. The holes in the elevator are approx. 03.-0.4mm oversize, the bottom hole in the torque tube is 0.7-0.8mm oversize. Advice the pilot gained from the manufacturer is that this slack/movement is not acceptable. Tecnam factory authorised repair scheme supplied for repair. |
27/10/2019 |
OCC1849 |
Bankstown Aerodrome |
NSW |
BRM Aero |
Bristell S-LSA |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Pre flight was conducted inside the hangar. The student was a...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Pre flight was conducted inside the hangar. The student was advised to not move the aircraft outside the hangar as per company policy while the instructor went into the office to do paperwork. The student proceeded to move the aircraft using the tow bar, and forgot to remove it resulting in the prop contacting the tow bar. |