Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
6/2/2020 |
OCC1949 |
Whitegum Aviation |
WA |
Micro Aviation |
Bat Hawk |
Camit |
3300SLRE |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: During annual inspection noted elevator control telef...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: During annual inspection noted elevator control teleflex cable inner guide tube has migrated out of the outer cable.
Guide tube was only held captive by rubber dust sleeve. |
3/2/2020 |
OCC1945 |
Noosa Heads |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After take off I was cleared by ATC to the north over water, ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: After take off I was cleared by ATC to the north over water, not above 1500 ft. I believed I had cleared the controlled zone at 1500 ft and started climbing to 3500 ft without a clearance over Noosa Heads. I believed I was out of the CTA step without looking at my maps. ATC called up on 126.7 advising that the aircraft had penetrated airspace at Noosa Heads.
The occurrence was reviewed by Operations for compliance. The pilot has subsequently undertaken a BFR and the incident was successfully reviewed with the school CFI. To prevent further occurrences the pilot will ensure maps confirm visibly recognised landmarks to ensure appropriate separation to airspace boundaries. |
1/2/2020 |
OCC1951 |
Shepparton Aerodrome |
VIC |
Tecnam |
P92 Echo Super |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During dual circuit lessons, at approx. 0.7 hr into the circu...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: During dual circuit lessons, at approx. 0.7 hr into the circuit during the downwind checks it was observed that the fuel burn was uneven in the fuel tanks. It was decided to address the imbalance by turning off the right hand tap allowing the left tank to be used for the remainder of the flight. The engine began to run rough then stopped after a couple of minutes.
The Instructor took immediate control of the aircraft, set glide speed and made decision that the aircraft was not within glide range of the runway. A suitable paddock was selected and a mayday call broadcast with intentions for the circuit traffic VH-ITY also on downwind for runway 18. Trouble checks were conducted finding that both fuel taps were set in the off position. Engine re-start was successful. Circuit was completed normally with a full stop landing.
The FTS has initiated a change to procedures preventing changes to the fuel taps during circuits.
This event is noted as occurring in Tecnam P92 on previous occasions with students and instructors due to the action of the taps on each door pillar.
Pilots are recommended to review the POH for the aircraft to familiarize themselves with the correct fuel tap positioning. |
29/1/2020 |
OCC1938 |
Taroom |
QLD |
Ercoupe |
415- C |
Continental |
C85 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After becoming disoriented to their location the pilot perfor...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: After becoming disoriented to their location the pilot performed a precautionary landing due to low fuel. The pilot was suffering dehydration which adversely affected their decision making. Investigation revealed that the pilot had an overdue BFR, required a medical declaration and aircraft registration was also overdue. The pilot certificate has been suspended until the pilot can undergo a BFR in addition to any other remedial training as required. Members are encouraged to use the Member App and Member Portal to ensure their compliance requirements including flight reviews, membership and aircraft registration are current and correct. Members are also encouraged to ensure appropriate flight planning is completed, including fuel management and consider the effects of dehydration when operating in hot climates and to have suitable amounts of water with them at all times. |
29/1/2020 |
OCC1943 |
Cape Barren Island |
TAS |
Jabiru |
J/120C |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Flying from Flinders Island to Tasmania, via Cape Barren Isla...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Flying from Flinders Island to Tasmania, via Cape Barren Island when the engine failed over water approximately five nautical miles South of Cape Barren Island. The airstrip on Cape Barren Island is on the Western side and the aircraft was positioned to the South. The pilot glided toward the airstrip, not expecting to get there, however, a dirt road ran from the south side of the island toward the airport. The pilot elected to land on the dirt road. The road was not wide enough for the wingspan and the right-hand wing impacted with the foliage spinning the aircraft 180 degrees. No injuries were incurred. On inspection of the engine, it was found that the exhaust valve on the number three cylinder had failed. |
29/1/2020 |
OCC1936 |
Lilydale Airport |
VIC |
Jabiru |
J160C |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Exhaust valves excessively leaking from CYL #3, 42/80...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Exhaust valves excessively leaking from CYL #3, 42/80psi, and CYL #4, 44/80psi |
28/1/2020 |
OCC1933 |
Lilydale Airport |
VIC |
Jabiru |
J160D |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Heavy Exhaust Valve leak from Cylinder #3. Compressio...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Heavy Exhaust Valve leak from Cylinder #3. Compression results 44/80psi |
27/1/2020 |
OCC1977 |
Caloundra Aerodrome |
QLD |
Pipistrel |
Virus SW 100 |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The Virus was taxiing and backtracking 05 behind a Cessna 172...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The Virus was taxiing and backtracking 05 behind a Cessna 172. When Cessna reached the threshold of the runway and turned 180 degrees to line up and take off, the Virus proceeded to taxi off to the right of the runway which required them to enter the grassed area off the side of the runway to allow the Cessna clearance to proceed to take off. As the pilot taxied over into the grassed area they struck a runway light with the propeller causing damage to one of the blades on the prop and rendering the aircraft unairworthy to fly. The light happened to be out of the pilots’ vision as the aircraft was centred on the trajectory towards the light and was in a blind spot to the ground, also the grass had not been mowed which had camouflaged the light. |
26/1/2020 |
OCC1932 |
Muchea Greenside ALA |
WA |
Jabiru |
J170C |
Jabiru |
2200 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The upper through bolt between #3 and #4 cylinder fai...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The upper through bolt between #3 and #4 cylinder failed at the point where the thread stops. |
26/1/2020 |
OCC1944 |
Aratula |
QLD |
Rainbow Aircraft |
Cheetah XLS (Bushcat) |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a group sortie to a private strip the pilot conducted ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a group sortie to a private strip the pilot conducted a stabilised approach but bounced on landing, during recovery actions the second touch down point was on a recently repaired softer section of the strip which caused the aircraft to skew left further impacting a tree stump and coming to rest on the left side of the landing area after further impacting trees. The pilot received serious but non life threatening injuries in the impact and the aircraft was severely damaged. The pilot has no recollection of the accident events but creditable witnesses confirmed the above information stating that during the bounce recovery the aircraft most likely stalled despite the use of power which added energy to the final impact. Other mechanical or environmental factors are not considered as contributing factors in this accident at this time. |
25/1/2020 |
OCC1940 |
Bendigo Aerodrome |
VIC |
Zenith Aircraft |
Zodiac CH 601 XL |
Jabiru |
3300cc |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Following a touch and go on RWY 35, upon contact to the RWY, ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Following a touch and go on RWY 35, upon contact to the RWY, the pilot proceeded to apply full power after which the engine surged and then cut off approximately three seconds later. At this point the aircraft was approximately halfway down the runway at 15ft AGL. The pilot applied nose down attitude and executed a flair and applied brakes until full stop. They were clear of any aircraft and managed to restart the engine and proceeded to the hanger.
Outcome: Once in the hanger they carried out basic trouble shooting and found fuel overflowing from carburettor inlet heading towards the air filter box. At this stage they were not sure as to what was causing this.
Next day the carburettor was stripped down and it was noted that a white silicon substance was lodged between the float valve and seat. Further investigation found that the silicon material had come from a fuel sender - this was discovered by cutting open the sender unit and finding the same material which was used by the manufacturer to attach the actual sensor. Of course, the silicon which was used was not AVGAS friendly even though the specification stated that it was fuel compatible. We have since removed any contaminants, by flushing the fuel line, removing the suspect fuel sender and completed a carburettor tear down. Engine is now fully functioning. Do not purchase any fuel related devices unless you have manufacturers specifications that the device is suitable for use in fuel related systems. |
25/1/2020 |
OCC1931 |
Gympie |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912IS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: A student on a solo training flight conducted a successful fo...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: A student on a solo training flight conducted a successful forced landing into a paddock. Review determined failure was caused due to failed alternator and suspect earth grounding issue. New firewall forward package installed. |
24/1/2020 |
OCC1946 |
Parkes Aerodrome |
NSW |
Flight Design |
CTMC |
Rotax |
912 U L S |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was pre-flighted and pulled from the hangar for ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was pre-flighted and pulled from the hangar for the first flight of the day. Run-ups were carried out in situ (without the need to taxi) and the student taxied across the apron and on to taxiway C (minimal rudder inputs required). As the aircraft entered and commenced the turn to back track to RWY 22 the student was unable to complete the turn, the Instructor took over and found they had full rudder travel but no response from the nose wheel. The Instructor gently manoeuvred the aircraft off the RWY beyond the gable markers leaving the RWY unobstructed for any other aircraft. |
24/1/2020 |
OCC1941 |
Caboolture |
QLD |
Tecnam |
P92 Echo S |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During the 3rd Pre-flight inspection of the day, the student ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: During the 3rd Pre-flight inspection of the day, the student identified a coolant leak from the #4 Cylinder head, upper coolant hose mating inlet fitting. The o-ring was replaced and an engine ground run carried out with no leak evident. Following a short test flight, the fitting was again inspected and found to be weeping. The seat of the cylinder head that houses the o-ring was inspected with a magnifier and a crack was found on the inner shoulder. The aircraft was removed from service and a serviceable cylinder head assy was obtained from the manufacturer. The Cylinder Head replaced IAW the Rotax Maintenance manual and test flown serviceable. |
23/1/2020 |
OCC1954 |
Chinchilla Aerodrome |
QLD |
Foxcon Aviation |
Terrier T100 |
Subaru |
Ea81 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot attempted 2-3 times to conduct an engine start, wit...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot attempted 2-3 times to conduct an engine start, with the difficulties attributed to the use of stale fuel. The engine subsequently had started at full power although the pilot does not recall setting full power. The pilot was able to throttle back and thought they had switched the ignition off but couldn’t prevent the aircraft from moving. It all happened in very quickly in an estimated 30 secs and the aircraft moved forward approx. 20 meters, colliding with a fence and avoiding a fuel truck. Nil injures were sustained, however there was damage to the wings of the aircraft.
The pilot will ensure consideration is given to the positioning of the aircraft, confirmation of throttle position, use of new fuel and use of switches to shut down the engine as part of every start. |