Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
9/1/2020 |
OCC1922 |
Warwick Aerodrome |
QLD |
Jabiru |
J 230 C |
Jabiru |
3300 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: When the aircraft was on late final at 50ft a Cockatoo struck...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: When the aircraft was on late final at 50ft a Cockatoo struck the port wing.
RAAus continues to monitor bird strike and wildlife reports at aerodromes to ensure correct ERSA/NOTAM information is in place and to enable reporting to the aerodrome proprietor. |
8/1/2020 |
OCC1926 |
Wingham |
NSW |
Rand Kar |
Hanuman |
Jabiru |
2200A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst taxiing for take off the pilot of the Hanuman ultralig...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst taxiing for take off the pilot of the Hanuman ultralight lost control due to an undetected local gust that was most likely a clear dust devil or thermal release, The aircraft was lifted and impacted a nearby barb wire fence. The brakes on the aircraft would not stop the aircraft due to limited traction at the time. The pilot was uninjured but the aircraft suffered significant damage. The local weather station recorded a 74kmh gust at the time which was not evident in the forecasts for the location. This event occurred in the height of a very volatile summer season with high temperatures, unpredictable winds and fires in the greater area at the time. Pilots should consider the "big picture" in relation to decisions to fly especially during times where there is a high likelihood of unpredictable local environmental conditions. |
7/1/2020 |
OCC1924 |
Lethbridge Airport |
VIC |
Skyfox Aviation |
CA25N Gazelle |
Rotax |
912 A3 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Normal movement of the engine cowling in flight allow...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Normal movement of the engine cowling in flight allows air (and potentially fumes, fluid smoke and/or flame, if present) from the engine compartment to enter the cabin. Ram air pressure under the cowling causes it to bulge slightly when in flight, creating gaps between the firewall and the cowling. The firewall seal design does not provide any flex to take up and block these gaps. This defect appears to be inherent in the design of the firewall seal. |
4/1/2020 |
OCC1916 |
Wagga Wagga Aerodrome |
NSW |
Tecnam |
P2002 |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After 1.3 hours of normal flight in the YSWG training area th...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: After 1.3 hours of normal flight in the YSWG training area the aircraft returned to the CCT where it conducted 2 go-arounds’ (only for training purposes) and on the 3rd it landed. As it came to a stop the pilot noted the nose tyre must have been low in pressure. Once it cleared the RWY the pilot stopped to inspect the aircraft and saw the nose tyre had deflated. The aircraft was tugged back to the hangar.
Outcome: No investigation required by RAAus. |
3/1/2020 |
OCC1914 |
Caboolture Aerodrome |
QLD |
Airborne |
Edge XT 912 |
Rotax |
912 UL |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Because of the pilots’ weight, (only 25 kg over the minimum f...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Because of the pilots’ weight, (only 25 kg over the minimum for the aircraft) additional ballast in the form of a punching bag weighing 50 kg is fitted in the back seat of the trike, which is restrained with the fitted inertia-reel seatbelt and a ratchet strap because the seat belt is not adequate on its own. The leftover tail of the ratchet strap was wound up and looped on itself the way truck drivers secure their straps, which results in a knotted loop of tape hanging from the ratchet. The nature of the ballast bag has meant that on occasion, the ratchet is to be re-tightened. The resulting extra length of tail was looped over the strap near one of its end hooks so only a short piece of tape with the knotted loop is hanging. It appears the extra tape unwound itself and the knotted loop was pulled to the rear by the Windstream. The tape melted on the exhaust pipe and the knotted loop detached and passed through the propeller. The pilot noted a bump as the leftover tail of the strap hit the propeller, but there was no further indication of damage. The pilot was only two miles from the airfield, so continued on and landed normally. The propeller sustained no damage, as evidenced by the 10 or so minutes the engine ran before the pilot could check what happened. There was no unusual vibration and a visual check shows no nicks or other damage. |
30/12/2019 |
OCC1917 |
Serpentine Aerodrome |
WA |
Ragwing |
RW11 Ragabond |
Great Plains |
2180 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was being test flown, it was fitted with a new e...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was being test flown, it was fitted with a new engine. During climb out a loss of power was experienced at 200 AGL. Due to the terrain being less than optimal for an emergency landing the aircraft was flown downwind along a fence line to attempt to make a base turn onto the originating airstrip. When it became clear that there was insufficient altitude or power available for the intended landing, the aircraft completed an outlanding in the only favourable paddock. This was accomplished with no damage to the airframe or pilot. On exiting the aircraft, it was noticed that a copious amount of oil was flowing out of the cowling. On review the engine appears to have suffered significant internal damage. The engine was compression tested showing complete lack of compression on one cylinder blowing air through the crankcase. |
28/12/2019 |
OCC1913 |
Moorabbin Aerodrome |
VIC |
BRM Aero |
Bristell S-LSA |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Student noted the master caution light come on and start flas...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Student noted the master caution light come on and start flashing. Passing the airport inbound reporting point, the student descended to 1000 feet approaching 3NM inbound and started noticing a blank noise. Student conducted radio failure check to confirm whether they actually had a failure or not. Student took it as a radio failure. Transmitting blind, they squawked 7600 then made call joining downwind RWY17R, did not hear any response. Joining base, the student heard static and then the tower respond and the radio came back live again. The student was advised to change transponder back to 3000 which they did and they were given landing clearance and landed safely. |
27/12/2019 |
OCC1953 |
Sunshine Coast Aerodrome |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a dual flight training exercise in the circuit area th...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a dual flight training exercise in the circuit area the tail of the aircraft stuck the ground during a touch & go. The aircraft had already conducted several touch and go's without incident with the student acting as pilot in command. Winds at the time were 7-10 kts from the East. The aircraft was configured for a crosswind landing with flaps at 10 degrees. During the landing flare the aircraft experienced a sudden high sink rate. The student correctly increased power to arrest the sink but unfortunately also raised the nose too high which resulted in the main gear and tail contacting the runaway simultaneously. The high sink rate occurred too quickly for the instructor to take over and correct the sink and high nose attitude. After the initial contact with the runway the aircraft became airborne again and the student called for a go-around. The instructor took over and elected to land and stop due to possible tail damage.
The CFI has since included advice to the Instructors, pilots and students alerting to the potential issues from the proximity of buildings in nominated winds. |
26/12/2019 |
OCC1910 |
Dublin Town |
TAS |
Just Aircraft |
Superstol |
Rotax |
914 UL2 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Abeam of Bicheno the Fuel Pressure light indicated red. The p...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Abeam of Bicheno the Fuel Pressure light indicated red. The pilot engaged the Auxiliary Fuel Pump and indicator returned to green. The pilot amended their flight plan to track direct to their home field. This was reported to Melbourne Centre (126.5 Mt Barrow) who undertook to monitor the remainder of the flight. Abeam Fingal the pressure indicator started to flash between green and red again, and so the pilot diverted directly to a nearby airfield. Over some very rough country the pressure indicator dropped dramatically and so the pilot decided to make a precautionary landing on the only cleared area they could find. The pilot declared a Mayday situation and Melbourne Centre monitored them through to the landing. The landing was with the wind, uphill and a little rough. This is a rugged bush aircraft and there is no obvious damage. Search and Rescue called the pilot on the phone, checked on their wellbeing and had them activate their emergency locator beacon. Once a position fix was made S&R despatched the local Fire Brigade to collect the pilot. Pilot revealed that the fuel pumps were contaminated with a sealant type product. The fuel system has been decontaminated and aircraft returned to service. |
23/12/2019 |
OCC1909 |
Castella |
VIC |
Zlin Aviation |
Shock Cub |
Rotax |
912 ULS2-01 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Shortly after departure from the Yarra Valley Estate whilst c...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Shortly after departure from the Yarra Valley Estate whilst climbing through approx. 2700ft AMSL and approaching the Glenburn gap the pilot noticed the oil pressure was decreasing and immediately initiated a 180 degree turn back towards the departure point. Within 15 secs the oil pressure had reached 0 and the engine came to a sudden stop. The pilot turned towards a cleared paddock and transmitted a Mayday call on YLIL CTAF then changed frequencies to Melbourne Centre and transmitted another mayday on 135.7 advising of the engine failure and that they were squawking IDENT on their transponder. The aircraft was landed successfully on the side of a gently sloping hill. The pilot then transmitted blind on 135.7 advising to cancel the Mayday and that the aircraft had landed safely. Cause:- Tthe
oil cooler outlet banjo fitting had come slightly loose and allowed the oil pump to suck air and cavitate |
23/12/2019 |
OCC1934 |
Lilydale Airport |
VIC |
Jabiru |
J160C |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Rocker bushings and rocker shafts on CYL #2 showing e...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Rocker bushings and rocker shafts on CYL #2 showing excessive wear |
20/12/2019 |
OCC1912 |
Narromine |
NSW |
Arion |
Lightning |
Jabiru |
3300 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Inadvertent flight into IMC: The aircraft departed Narromine ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Inadvertent flight into IMC: The aircraft departed Narromine into significant smoke haze. At 500' the pilot could see objects out to about 10NM but could not see the horizon. At cruise altitude of 4,500' visibility became worse. The visual cues indicating the aircraft's attitude became degraded. The pilot could judge pitch and roll only by looking at the paddocks and roads within a 45 degree cone beneath the aircraft. While the pilot was reviewing the latest weather details for Griffith the pilot realised the aircraft was in a 15 degree bank. The pilot then engaged the autopilot to ensure the aircraft maintained wings level.
The smoke progressively thinned out towards Griffith and visibility entering the circuit was satisfactory until initiating their turn to base. During this descent the aircraft encountered a lens of smoke which totally blocked the view of the runway ahead, while view of crosswind and downwind remained relatively clear. The pilot estimated where the extended centreline of the runway was and turned final only to find, when exiting the smoke lens, that they had turned too soon, requiring a dog-leg correction to get back on the centreline.
RAAus has provided a range of educational information and guidance in relation to the difficulties of operating in areas of bushfire smoke and encourage pilots to ensure minimum visibility for VFR is maintained. |
19/12/2019 |
OCC1905 |
Tyagarah Aerodrome |
NSW |
Skyfox Aviation |
CA22 |
Rotax |
912 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Upon touchdown the aircraft veered to the left. The turn coul...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Upon touchdown the aircraft veered to the left. The turn could not be arrested and the aircraft contacted scrub on the side of the strip.
The rudder horn failed to contact the control stop, as it passed the increased leverage placed on its attachment point causing it to bend to a point where no rudder movement to starboard was possible. This caused a loss of directional control leading to an impact with debris on the side of the runway. The starboard brake assembly was ineffective as debris on the side of the runway tore the fluid feed line from the caliper. |
17/12/2019 |
OCC1902 |
Lilydale |
VIC |
Jabiru |
J-160-D |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Cylinder #1 and 2 Exhaust Valves leaking. Found durin...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Cylinder #1 and 2 Exhaust Valves leaking. Found during Compression test. |
17/12/2019 |
OCC1904 |
Lilydale Airport |
VIC |
Jabiru |
J-160-D |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Valve Rocker Bushes and Shafts have excessive wear
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