Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
1/11/2019 |
OCC1854 |
Bankstown Aerodrome |
NSW |
Aeroprakt |
A22LS Foxbat |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The nose wheel of the aircraft collapsed upon landing. The pi...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The nose wheel of the aircraft collapsed upon landing. The pilot went around, assessed the issue and landed safely.The report was investigated reviewing both operational and technical elements. Maintenance, airworthiness and other technical considerations were ruled out and the most likely identified primary cause was aircraft control management during landing.The flight school was contacted to request a review of the pilots training and performance which was completed.. |
1/11/2019 |
OCC1853 |
Bowen Aerodrome |
QLD |
ICP |
Savannah S |
Savannah |
SVG |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft is reported to have taken off and then landed th...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft is reported to have taken off and then landed the next day without making any radio calls. As the aircraft landed there was a local skydive aircraft with 5 people on board in the air ready to drop skydivers.
Further investigation revealed the pilot had flown into the CTAF without a working radio. The aerodrome has a radio carriage and use requirement.
The pilot is undertaking retraining with a RAAus CFI regarding these requirements. |
27/10/2019 |
OCC1851 |
Greenside ALA |
WA |
ICP |
Savannah VG |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The Trim tab was able to move freely up and down appr...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The Trim tab was able to move freely up and down approx. 10 - 12 mm. This caused the aircraft's elevator to be neutrally stable to marginally unstable if the control column was released during flight, and this effect was exacerbated due to light air turbulence.
Upon inspection the actuation / trim control system was found to be loose with rod ends indicating wear. The trim tab control bell crank was also loose and allowed some additional play of the trim tab. There was also some looseness of the trim tab piano hinge due to narrow gauge wire in the hinge.
Worn components, checking for wear and play in the controls systems is a requirement during the 100/ annual inspection. |
27/10/2019 |
OCC1863 |
Palmyra Airstrip |
QLD |
Tecnam |
P92 Eaglet |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Whilst completing a pre-flight inspection, the pilot ...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Whilst completing a pre-flight inspection, the pilot detected movement in the LH elevator (up/down and fore/aft). An L2 was called and they determined that the movement was from within the elevator itself. The LH elevator was removed and it was found that the holes in the torque tube and the elevator had been drilled oversize. There is a single M8 bolt inside a 10mm OD bush holding the elevator halve to the torque tube. The holes in the elevator are approx. 03.-0.4mm oversize, the bottom hole in the torque tube is 0.7-0.8mm oversize. Advice the pilot gained from the manufacturer is that this slack/movement is not acceptable. Tecnam factory authorised repair scheme supplied for repair. |
27/10/2019 |
OCC1849 |
Bankstown Aerodrome |
NSW |
BRM Aero |
Bristell S-LSA |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Pre flight was conducted inside the hangar. The student was a...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Pre flight was conducted inside the hangar. The student was advised to not move the aircraft outside the hangar as per company policy while the instructor went into the office to do paperwork. The student proceeded to move the aircraft using the tow bar, and forgot to remove it resulting in the prop contacting the tow bar. |
25/10/2019 |
OCC1894 |
Caboolture |
QLD |
Tecnam |
P92 Echo S |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: During an aircraft refurbishment the screws holding t...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: During an aircraft refurbishment the screws holding the vertical stabiliser fairing on were severely corroded. Upon removal the upper rib had extensive corrosion and needed to be replaced. As the upper rib also housed the upper rudder attachment, all attaching parts were also replaced with new from manufacturer. |
24/10/2019 |
OCC1846 |
Monbulk |
VIC |
Jabiru |
J160D |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a routine training flight conducting ab initio trainin...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a routine training flight conducting ab initio training with a student pilot, the oil inspection cover plate detached quickly from the aircraft. The cover plate did not contact any part of the aircraft when it detached. The pilot returned for a landing without incident. It is unclear whether the cover plate hinge screws were loose or if they vibrated loose in flight. RAAus reminds members to carry out thorough preflight checks. |
20/10/2019 |
OCC1844 |
Goulburn Aerodrome |
NSW |
Skyfox |
CA25N Gazelle |
Rotax |
912A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot neglected to return to CTAF after checking the AWIS...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot neglected to return to CTAF after checking the AWIS. The pilot performed visual checks for the intended runway and in the absence of radio traffic, broadcast his intentions to line up and depart. As a result an aircraft on final was forced to abort its landing. The pilot aborted the take off and returned to the hangar. Subsequently the pilot was counseled by the CFI regarding the importance of extended visual checks for fast incoming aircraft and ensuring the radio was operated on the correct frequency. |
20/10/2019 |
OCC1848 |
Emkaytee |
NT |
ICP |
Savannah XL |
Rotax |
912 ULS |
Fatal Accident involving RAAus member. RAAus accident consultants are assisting police in determinin...
|
Fatal Accident involving RAAus member. RAAus accident consultants are assisting police in determining the causal factors that led to the accident. |
20/10/2019 |
OCC1842 |
Bankstown Aerodrome |
NSW |
Tecnam |
P2008 DL LSA |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After a go around on runway 29R, the student, who was conduct...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After a go around on runway 29R, the student, who was conducting a training area solo, became concerned about a helicopter in the helicopter circuit and subsequently made a left hand circuit instead of a right hand circuit.
There was no imminent collision, but it was contrary to the aerodrome procedures.The incident was reviewed with school CFI as part of an ongoing training standards review process. |
20/10/2019 |
OCC1845 |
Minlaton Aerodrome |
SA |
Jabiru |
SP500 |
Jabiru |
2200A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was conducting a touch and go landing and decided a...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was conducting a touch and go landing and decided at approximately 20 ft to go around as they were not aligned with strip. The power was removed in error resulting in no time to recover. This resulted in a very heavy landing with the nose wheel and one main leg collapsing, however due to low speed the aircraft only skidded approx. 6m.
The pilot provided a response indicating in the future an earlier decision to conduct a go-around will be enacted. |
19/10/2019 |
OCC1843 |
Narromine Aerodrome |
NSW |
Morgan Aeroworks |
Cheetah Mk1 |
Jabiru |
2200 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was flying into the airfield for a fly in and there...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was flying into the airfield for a fly in and there were a number of other aircraft in the circuit. The approach speed was too high on the first landing attempt and the aircraft bounced on contact. The pilot applied full power and elected to go around. On the second attempt the approach speed was correct and the runway was lined up, throttle was reduced to ideal, the aircraft touched down with a slight bounce, the pilot noticed that the throttle had increased so reduced it back to idle and held the nose up to wash off speed. The pilot looked out the window to assess height off the ground and felt the back wheels touch (at 48 knots). The aircraft drifted to the left side of the runway and the aircraft made a sharp left movement exiting the runway. The left wing and the nose wheel contacted the ground. The pilot is unsure if the sharp left movement was caused by the passengers leg hitting the control stick or a subconscious input by the pilot who had learned to fly in trikes. By this stage the aircraft was off the runway, power was applied to straighten the path, however the nose wheel collapsed and aircraft slid to a stop after 30 to 40 metres.
The pilot was requested to complete a flight review to ensure correct control inputs are made and possible go-around actions in the future are understood. |
17/10/2019 |
OCC1838 |
Bankstown Aerodrome |
NSW |
Sling |
2 |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: An Instructor and Student were conducting a lesson of circuit...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: An Instructor and Student were conducting a lesson of circuits on RWY 29L. The engine had been running with no issues, ground run and checks indicated no issues. After 4 normal circuits the student increased power and raised the nose to take off when just past the end of the RWY at approx. 520ft the engine had rough running indications at 4200 RPM. The Instructor took over and landed RWY 11L with no issues. Cause unknown, pilot and engineers unable to replicate fault. |
17/10/2019 |
OCC1840 |
Sunshine Coast Aerodrome |
QLD |
Flight Design |
CTLS |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was tracking northbound coastal from Caloundra to N...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was tracking northbound coastal from Caloundra to Noosa Heads. Clearance was obtained to track via the coastal route at 1500 ft. The pilot was instructed to advise YBSU tower when clear of controlled airspace. The pilot thought controlled airspace extended to Noosa Heads, but it actually ended at the CTA boundary. The pilot was advised by YBSU Tower that they had been detected clear of controlled airspace and that frequency change was approved. The pilot acknowledged, checked location on VTC, noted that they were still under the Class D 1500-4500 step, and commenced a left turn to clear the control step. The pilot commenced a climb but failed to confirm that they were over land and clear of the control step before doing so. The pilot therefore entered Class D airspace for a short period without clearance. ATC advised the aircraft had climbed to 1900' AMSL prior to boundary.
The pilot undertook remedial training with a CFI to ensure understanding of controlled airspace assessment and avoidance was clear. |
13/10/2019 |
OCC1830 |
Bendigo Aerodrome |
VIC |
Tecnam |
P92 Echo Super |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst returning the aircraft to the hangar manually/pushing ...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst returning the aircraft to the hangar manually/pushing back, the outer trailing edge of left wing impacted hangar door.
When moving aircraft it is essential to maintain awareness of surroundings. |