Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
20/6/2020 |
OCC2050 |
Nobby |
QLD |
Eastwood Aircraft |
Tyro MkII |
Rotax |
447 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft departed with 25L of fuel on board. A 50-minute ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft departed with 25L of fuel on board. A 50-minute flight was conducted before engine stopped. The aircraft landed safely in a paddock.
Outcome: The rubber on the inside of the fuel hose supplying the carburettor was found to have degraded causing a blockage. |
19/6/2020 |
OCC2051 |
Packsaddle Station |
NSW |
Aeroprakt |
Foxbat |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft operated for 3 hours on the morning of the incid...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft operated for 3 hours on the morning of the incident. It refueled, the fuel was checked for contaminates after refueling. The aircraft departed for another station 120nm south of Packsaddle. The engine failed after take-off at 400ft AGL. The pilot tried to restart it but was unsuccessful. The aircraft landed in a cleared area of the paddock.
Review identified failure was likely due to fuel contamination as the aircraft was refueled from a fuel drum on a farm. Since the incident fuel management and testing procedures have been improved to prevent a repeat occurrence. Members are reminded of the importance of proper fuel management ensuring fuel is not contaminated prior to use. |
19/6/2020 |
OCC2063 |
Monomeith Park Airfield |
VIC |
Jabiru |
J160C |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Cylinder #3 Exhaust Valve failed.
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18/6/2020 |
OCC2047 |
Koo Wee Rup |
VIC |
Jabiru |
J160C |
Jabiru |
Gen 4 2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During dual navex flight training a small loss of power was ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: During dual navex flight training a small loss of power was noticed, 50-100rpm or so. The instructor suspected maybe carby ice, however carby heat made no difference so removed the CH. About 30s-1 min later the aircraft experienced a sudden onset of severe vibration and loss of power - it felt like a cylinder had stopped, the instructor took over at this point. Reducing throttle to below 2000rpm got rid of the vibration a bit. Adding it back and the engine immediately started to vibrate badly and clearly not run on all 4. The aircraft had insufficient power to maintain altitude. The instructor chose a field to make an emergency landing whilst trying carby heat, fuel pump and mags to no avail. The aircraft landed uneventfully. |
18/6/2020 |
OCC2049 |
Bankstown Aerodrome |
NSW |
Jabiru |
J170-D |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Touchdown on RW29R was normal, but during the rollout, the ai...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Touchdown on RW29R was normal, but during the rollout, the aircraft tended to veer to the left.
When moderate braking was applied, and Aircraft tracking corrected, the Brake lever went completely slack and Braking action was lost completely.
After exiting the runway, there was a tendency to track to the left and i felt that the left brake was dragging however i was able to taxi back to the hangar under power without assistance. |
16/6/2020 |
OCC2119 |
Mallacoota |
VIC |
FK Lightplanes |
FK9 WB |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The electric elevator trim control appeared to be not working...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The electric elevator trim control appeared to be not working or very slow in flight. The trim position indicator on the Garmin G3X display confirmed little movement of the elevator. The elevator on this aircraft is a flying surface, there is no trim tab fitted.
Subsequent ground inspection showed that when the stick mounted trim button was operated, there was no movement in the elevator when any force was exerted on the stick. If the stick was not loaded (no force applied) the trim button did move the elevator very slowly.
A flight test was conducted which again confirmed the original observation. During the test, the Garmin Autopilot was engaged. The Flight Display showed TRIM UP & TRIM DOWN flags at various times in the flight, operating the trim control did not cause the pitch to change or the flag to be removed. |
14/6/2020 |
OCC2072 |
Balingup |
WA |
Skyfox |
CA22 |
Rotax |
912A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft landed successfully on a private strip, however ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft landed successfully on a private strip, however during landing roll the propellor made contact with a sheep fence at approx. 20-30kmph. RAAus investigations determined the pilot was not a current member, had not completed a BFR and the aircraft was not registered at the time of the flight. The pilot was aware of these non-compliances, yet continued with the flight regardless. He has now been suspended pending completion of requirements to address the non-compliances. Members are reminded there may be serious consequences to operating outside the RAAus Flight Operations and Technical Manuals, including insurance implications, disciplinary action by RAAus and CASA and potential convictions as a result of breaches of the Civil Aviation Act (1988). |
13/6/2020 |
OCC2046 |
Yarram |
VIC |
Zenith |
Zodiac CH 601 HD |
Subaru |
EA81 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft departed Yarram airport and headed to the south ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft departed Yarram airport and headed to the south east of the field. Upon reaching the coast it was noticed that engine coolant was coming out from the engine cowling and dripping onto the dashboard, the pilot turned the aircraft around to head back to the airport. Shortly after turning back smoke started to fill the cockpit so the pilot called Yarram’s frequency to advise aircraft was experiencing engine troubles and was intending to return to the airport. As more smoke filled the cockpit the pilot opened the latch to their side of the canopy in an attempt to let some of the smoke out, it helped however visibility was still impaired.
When the aircraft was approx. 2 miles from the strip the engine started to seize and had no power. The passenger (also a pilot) attempted to land the aircraft in a clearing in front of them, as the pilot could not see clearly due to fogged glasses. Just before the clearing they saw a glimpse of the tree canopy through the smoke and realised that we were not going to make it. The aircraft then made contact with and remained suspended in trees approx. 7m above the ground. One occupant fell to the ground and the other managed to climb safely to the ground.
During the review it was not possible to determine the cause of the failure. Pilots are reminded to consider a precautionary landing rather than trying to press on to an airport when experiencing technical issues. |
10/6/2020 |
OCC2038 |
Aldinga Aerodrome |
SA |
Evektor |
Harmony |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: A solo student landed on runway 03 and turned around to backt...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: A solo student landed on runway 03 and turned around to backtrack. Another aircraft was on final approach to runway 03. A pilot in another aircraft in the circuit called over the radio for the aircraft on final to go around but the aircraft was committed to land and the pilot determined there was insufficient runway to safely complete a go around. The aircraft continued to land on the occupied runway and vacated the runway well clear of the solo student.
No backtracking call was made by the solo student and during a debrief it was acknowledged the pilot of the second aircraft would consider a go around in similar circumstances if sufficient runway remained to safely do so.
Pilots are reminded of the importance of ensuring a runway is clear prior to landing as outlined in CAR166 and conducting a go around if the runway is not clear. |
9/6/2020 |
OCC2034 |
Sunshine Coast |
QLD |
Tecnam |
P2002 JF |
Rotax |
912 - S - 2 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft inadvertently penetrated controlled airspace. Th...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft inadvertently penetrated controlled airspace. The pilot acknowledged the use of out of date charts and will ensure for any future flights current information is accessed as part of the planning phase. Pilots are reminded of the importance of maintaining up to date charts as well as thorough pre-flight planning to remain clear of controlled airspace. |
9/6/2020 |
OCC2042 |
Redcliffe Aerodrome |
QLD |
Tecnam |
P92 Eaglet |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: A dual instructional flight was returning from the Bribie Isl...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: A dual instructional flight was returning from the Bribie Island training area and overhead Beachmere the student made a reporting call, as per protocol reporting position and intentions, when they heard another aircraft report to being in the same area and with the similar intentions. Not having this aircraft visual they requested more location information, which the pilot of the VH registered aircraft supplied and visual contact was then made and confirmed by both aircraft.
As the Tecnam approached YRED they had lost visual of the VH aircraft and continued their overhead approach for runway 25, as this runway is a right hand circuit and requires all turns within the circuit area (3NM of the runway) to be right hand turns. The student reported their position as being overhead the field at 1500 ft and announced their intention was on descent to join crosswind for runway 25 and commenced a right hand descending turn to join crosswind at 1010 ft.
About part way through the right hand descending turn the instructor and student observed the pilot of VH aircraft conducting a left hand turn and noted the two aircraft were on a collision course. The Tecnam took immediate avoiding action to prevent a collision between the two aircraft. The Tecnam continued their descent and joined midfield downwind, landing without further incident.
During the review, this information was forwarded to CASA for review as this involved a VH registered aircraft. Pilots are reminded of the importance of maintaining standard procedures when operating at uncontrolled aerodromes as well as maintaining active radio calls in order to build a picture of the location and intentions of other traffic in the area. A good lookout must always be maintained to avoid the risk of a near miss occurrence. |
6/6/2020 |
OCC2033 |
Serpentine Aerodrome |
WA |
Kolb |
Xtra Mark III |
Rotax |
912S |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was test flying the kit built aircraft, the first t...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was test flying the kit built aircraft, the first touch and go was completed without incident on a sealed runway. The second circuit was completed with a touch and go on the grass runway. After applying power and climbing everything was normal until around 175ft above ground when significant rudder aerodynamic flutter began. With airspeed at 80mph the nose was pushed forward while reducing power the rudder pedals were oscillating severely and could not be contained. The pilot momentarily removed their feet from the rudder pedals to see if it would settle, the flutter continued. The stick was stable with no vibration. The engine was cut to idle the rudder flutter continued. The rear of the aircraft was now vibrating the whole airframe and the pilot chose to push the plane back onto the ground.
Touching down at high speed approx. 125ft before the boundary fence, full brakes were applied and the pilot attempted to ground loop the aircraft to avoid or lessen the impact with the boundary fence. Approx. 20ft from the fence the left rudder pedal broke off under the high pressure of braking. The aircraft veered approx. 90 degrees to the right and impacted the corner section of the boundary fence. The nose impacted one of the three posts and the wing strut impacting the rail between the other two posts. The tail impacted the wire fence breaking the left stabiliser off the tubular boom and severely damaging the lower part of the rudder.
The nose was crushed up to the pilots’ feet. On impact the throttle was advanced due to the inertia of the impact the pilot immediately reduced the power to idle and went through the shutdown procedures. |
6/6/2020 |
OCC2041 |
Temora Aerodrome |
NSW |
Jabiru |
160C |
Camit |
2200 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: As the aircraft was turning to park, the left wingtip contact...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: As the aircraft was turning to park, the left wingtip contacted the aero clubs’ veranda pole.
Members are reminded to maintain a constant lookout during ground handling and to ensure that aircraft are checked by an appropriate maintainer following occurrences of this nature. |
5/6/2020 |
OCC2043 |
Redcliffe Aerodrome |
QLD |
Tecnam |
P92 Eaglet |
Rotax |
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst an instructor and student pilot were conducting pre-f...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst an instructor and student pilot were conducting pre-flight checks in the designated run-up area, they heard an incoming VH registered aircraft announce that they were going to execute a “Straight in approach” in Redcliffe aerodrome. The ERSA states in item 6 of the Noise Abatement section pertaining to YRED that “No straight in approaches are permitted at YRED”.
This occurrence was submitted to CASA for follow-up. Members are reminded to review and follow appropriate aerodrome procedures prior to operation. |
1/6/2020 |
OCC2048 |
Tumut Aerodrome |
NSW |
Two Seat Bi-plane |
Barnstormer |
Rotec |
R2800 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was being test flown and had done approx. 4 hour...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was being test flown and had done approx. 4 hours at the time. It was at 1200ft and overhead the airfield at the time when the pilot felt a slight hiccup in the engine. The pilot managed return and land safely then taxi back to the hangar. Upon investigation it was found that the number 5 cylinder piston connecting rod had disintegrated into 5 separate pieces and done severe damage to the lower cylinder barrel and crank case. |