Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
9/12/2022 |
OCC3060 |
Gawler |
SA |
Jabiru |
J170 |
Jabiru |
2200B |
STATUS: Review Complete
During dual circuit training, the conditions were gusty with a slight XW...
|
STATUS: Review Complete
During dual circuit training, the conditions were gusty with a slight XW. The student conducted the take-off and flew the initial circuit but was not maintaining attitude, so the instructor took over to demonstrate the circuit. When instructor took over, they noted degraded aircraft climb performance. The instructor flew the remainder of the low level circuit for a full stop. Investigation on the ground identified the hose for the cold air intake had dislodged. |
6/12/2022 |
OCC3058 |
Cessnock Airport |
NSW |
Legend |
600L |
Rotax |
912 ULS |
STATUS: COMPLETED
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft had landed at YCNK and was...
|
STATUS: COMPLETED
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft had landed at YCNK and was coming to a full stop. During the roll/taxi along the YCNK 17 runway the left wheel struck an lip in the runway surface located approximately 150meters from the threshold of 17. This uneven section of runway stuck the left wheel and caused the left wheel spat to crack and become dislodged from the aircraft. There was no other damage to the aircraft or any persons and the spat was removed from the runway.
OUTCOME: RAAus contacted the YCNK operator and spoke with the ARO who confirmed the incident. The ARO advised that the runway was due for major rework on the 19th of January 2023 and this would include a fix for the lip located on runway 17. Requested that the ARO add a NOTAM if possible, to warn other aircraft with small wheels and tightly fitted spats about the issues so that they could land long and avoid this section of the runway until such time as the runway was repaired. |
5/12/2022 |
OCC3090 |
West of Broadford |
VIC |
Pioneer 300 |
Hawk |
Rotax |
912 ULS |
STATUS: Under review
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst Climbing to avoid Cumulus Cl...
|
STATUS: Under review
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst Climbing to avoid Cumulus Clouds the aircraft infringed the CTA step of 4500 ft. It was an error regarding location in relation to the CTA step. After contact with ATC, the CTA was cleared as soon as it was possible. |
4/12/2022 |
OCC3064 |
Camden |
NSW |
Sonex |
Legacy |
Rotax |
912 ULS |
STATUS: Review Complete
During the second flight of an experimental aircraft the oil temperature ...
|
STATUS: Review Complete
During the second flight of an experimental aircraft the oil temperature was indicating to be outside acceptable parameters. The aircraft landed immediately, with assistance of ATC, without further incident.
The in flight cowling air flow was found to be inadequate. Modifications to cowling have been implemented and tested with engine temperatures now within the manufacturers specifications. |
3/12/2022 |
OCC3056 |
South East of Muswellbrook |
NSW |
Bristell NG5 |
S-LSA |
Rotax |
912 ULS |
STATUS: Review complete.
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was tracking BAXT to ...
|
STATUS: Review complete.
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was tracking BAXT to YSCO at 2500 feet. Approx. 25nm south of Scone, an unusual noise developed in the aircraft and got progressively worse over a period of approximately three minutes. Power was reduced and a severe vibration commenced. A call was placed to Brisbane Centre that the aircraft was experiencing difficulties and would be immediately commencing a precautionary search and landing. Once established on the ground and about 80 meters into the roll-out, several kangaroos came across the road and one or maybe two were struck by the left wing of the aircraft. This placed the aircraft into a sliding rotation and the right wing struck the embankment which resulted in the aircraft rotating further and coming to rest against the embankment at 90 degrees. The impact with the kangaroo's caused the nose-wheel to collapse and the left main gear to be damaged in the table-drain. The pilot shut down all systems and exited the aircraft uninjured.
OUTCOME. Aircraft was found to contain a substantial amount of contaminated fuel, which is likely to have caused the aircraft engine to suffer a loss of power. The amount of water contained in the fuel tank would have resulted in a fuel drain showing no distinction in color. This may have lead the pilot to believe that the fuel in the main tanks was not contaminated as there was no change in color between the water and fuel. |
2/12/2022 |
OCC3065 |
Off the end of R31 YGAW into EDN CTR |
SA |
Jabiru |
J170-C |
Jabiru |
2200B |
STATUS: REVIEW COMPLETE. Airspace infringement.
|
2/12/2022 |
OCC3068 |
Gawler |
SA |
Jabiru |
J170-C |
Jabiru |
2200B |
STATUS: REVIEW COMPLETE. Airspace infringement.
|
26/11/2022 |
OCC3046 |
PKR180004 |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912 |
STATUS: Under review
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After conducting simulated partial en...
|
STATUS: Under review
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After conducting simulated partial engine failure and forced landing training, a non-simulated loss of rpm and rough running occurred in the YBAF southern training area. After circling over suitable landing areas to troubleshoot, the pilot returned to YBAF in a shallow climb to increase options in the event of a total failure. The pilot conducted an upwind join and close circuit to land uneventfully RWY 28L. |
26/11/2022 |
OCC3048 |
Canberra Airport |
ACT |
Jabiru |
J160-D |
Jabiru |
2200-B |
STATUS: COMPLETE.
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Radio problem after departure from Canbe...
|
STATUS: COMPLETE.
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Radio problem after departure from Canberra. On ground radio was working fine and clearance was able to be obtained without issue. After departure passing 1000' as Canberra tower was handing aircraft off to approach the pilot noticed some crackling in the radio and didn't make out all of the handoff call. Readback was carried out but was said to be unreadable from Canberra tower. Subsequent call was made by the pilot asking for a return to the field and enough of this transmission went through that tower was able to coordinate them. Subsequent transmissions from the aircraft were completely unreadable however inbound transmissions were still received at readability 3. Aircraft made a safe landing and was grounded pending inspection.
OUTCOME: Aircraft has been repaired by a L2, including removing replacing a faulty cable and solder joints. Aircraft radio has since been tested both on the ground and in the air and found to be working correctly. |
26/11/2022 |
OCC3045 |
Archerfield Airport |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912 ULS |
STATUS: Under review
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was conducting circuits at ...
|
STATUS: Under review
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was conducting circuits at YBAF when a partial engine failure occurred. No issues were noted during run up. On first circuit, there were no issues, all went as per a normal circuit.
On take-off for the second circuit, the aircraft initially was performing normally. At approx. 400 feet, serious vibrations were felt, and the engine would not reach max climb power (max rpm noted was 4995rpm), normal climb power is 5200-5300rpm. The engine issue/incident was reported to the tower, as aircraft was approaching downwind, it stabilized at 5000PM before landing uneventfully. |
25/11/2022 |
OCC3049 |
Caloundra |
QLD |
Aeroprakt |
A22LS |
Rotax |
912 ULS |
STATUS: Review Complete
Determined Outcome: Whilst conducting a Nav flight with a student, the st...
|
STATUS: Review Complete
Determined Outcome: Whilst conducting a Nav flight with a student, the student conducted a supervised pre-flight on the aircraft and there was sufficient oil and fuel on board for the exercise. A touch and go was completed and the aircraft climbed out at 65 knots with full power. At 300ft AGL the engine started to sputter (multiple times). The Instructor noticed that the RPM was fluctuating and there was a vibration (similar to a wheel shimmy but in flight) in the aircraft.
The instructor then took over control from the student and tried to get as much height possible for a turn back to the field. Close to the ground the engine sputtered again.
After an extensive investigation, it was found that the right-hand fuel tank contained foreign matter which would intermittently block the fuel pick up port. The tank was removed, cleaned and reinstalled with no further defects evident. |
23/11/2022 |
OCC3043 |
Port Macquarie |
NSW |
Brumby |
R610 |
Rotax |
912 ULS |
STATUS: Review Complete
OCCURRENCE DETAILS SUBMITTED TO RAAUS: On climb out after take-off at appr...
|
STATUS: Review Complete
OCCURRENCE DETAILS SUBMITTED TO RAAUS: On climb out after take-off at approx. 150' the aircraft started losing power and vibrations could be felt through the airframe and control column. RPM decreased from approx. 5200 RPM to 4800 RPM initially and then gradually continued to decrease from there. The aircraft was able to maintain height at around 300' with partial engine power and the instructor opted to turn back on to the reciprocal runway. The aircraft was landed safely without further incident and the aircraft was subsequently grounded pending LAME inspection.
Determined Outcome: Borescope of number 1 cylinder found that the exhaust valve had failed. Valve renewed with nil further defects. |
20/11/2022 |
OCC3037 |
Muchea/Greenside |
WA |
Jabiru |
J170-C |
Jabiru |
2200 |
STATUS: Under review
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Defect: The suspension bungee appears...
|
STATUS: Under review
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Defect: The suspension bungee appears to have partially failed on the aircraft. |
19/11/2022 |
OCC3035 |
Ballarat Airport |
VIC |
Tecnam |
P2002 Sierra |
Rotax |
912 ULS |
STATUS: Review Complete
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Instructor and student noticed unus...
|
STATUS: Review Complete
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Instructor and student noticed unusual nosewheel shimmy during a lesson of touch 'n go circuits. They elected to call for a full-stop landing and to end the lesson. Once the aircraft had landed on the active runway, lack of directional control noted by the instructor who took control of the aircraft. The instructor established control and taxied clear of the runway.
Determined Outcome: Once the aircraft was shutdown it was noted that the front nosewheel tube had deflated. The aircraft and the rim of the tyre sustained no damage. |
16/11/2022 |
OCC3034 |
Pentland |
QLD |
Jabiru |
J200-B |
Jabiru |
3300 |
STATUS: Under review
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After fuelling at Hughenden, the airc...
|
STATUS: Under review
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After fuelling at Hughenden, the aircraft left for the return flight to Donnington. The pilot landed at Pentland for a break and there was no indication of fault of aircraft or engine.
After following the shutdown and removing their headset the pilot heard a very slight trickle/creak type sound. Being that it’s hard to look fully into the back of plane whilst seated and because they felt they should move with haste the pilot got out. Leaning through the door and looking into the back and pulling out the headset at the same time the pilot caught a glimpse of a flash up close to the back of the seat. Knowing that fuel lines run across the base of the seats in back they immediately got away from the plane and only was able to take the headset and bag from the passenger seat with them. Nothing seemed to be happening and the pilot thought if it’s a small fire they could use dirt to put it out. They then approached the back door and opened it but then could see that they couldn’t stop it. It looked like the area behind seat was alight. Emergency services were called to extinguish the fire. |