Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
8/10/2020 |
OCC2173 |
Caboolture Aerodrome |
QLD |
Aeropro |
2K Eurofox |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: An Instructor was flying circuits with a student on RWY 30. T...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: An Instructor was flying circuits with a student on RWY 30. They were established on final approach when they heard a radio call of an aircraft (C172) turning final. They were about 250 feet and assumed the second aircraft was higher and behind them. However very shortly after this radio call the C172 flew over the top of them while turning onto a short final. A R22 helicopter was hovering off to the side of the runway. The helicopter pilot alerted the pilot of the C172 that there was an aircraft beneath them and the C172 pilot executed a go-around. |
7/10/2020 |
OCC2148 |
Cessnock Aerodrome |
NSW |
TL Ultralight |
TL-3000 Sirius |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After conducting a solo check ride with the student the instr...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: After conducting a solo check ride with the student the instructor sent them for solo circuits. While taxing the aircraft the student failed to maintain directional control and caused the aircraft to leave the taxi way and roll into a ditch causing a prop strike and the aircraft to come to a stop with nil injury to the student. the aircraft has a castoring nosewheel, which may have been a contributing factor in the loss of control. An assessment of the student following the incident was completed and any required remedial training was carried out. |
6/10/2020 |
OCC2145 |
Iveragh Aerodrome |
QLD |
Aeroprakt |
A22LS Foxbat |
Rotax |
R-912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft made a straight in approach to runway 13 for a “...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft made a straight in approach to runway 13 for a “Touch and Go” and was attempting a Full Stop landing on the second circuit. The wind had dropped off and was almost flat calm on the second approach. The approach was a bit high and the aircraft floated more than usual. The flare was also high and aircraft drifted to the left. As the pilot decided to go around, the aircraft sank heavily onto the runway and bounced to the left, becoming entangled in the barbed wire fence at the side of the runway and coming to an abrupt stop. The pilot was unhurt and was able to turn off fuel, radio and electrics and exit the aircraft via the right side (passenger) door, because the LH door was obstructed by barbed wire. The barbed wire fence had to be cut away to extract the aircraft.
Subsequent to this accident the pilot undertook a review flight with an RAAus examiner at the same landing area and it was determined that the pilot did not recognise a quartering tail wind effect at the beginning of the threshold, believed to be caused by high cane field crops on the approach to the SE runway. It was recommended that future landings move the initial aiming point further into the available landing area which was more than adequate for the aircraft type. Delayed reactions and decision making were also identified as further contributing factors to this event. |
5/10/2020 |
OCC2144 |
Warwick Aerodrome |
QLD |
Europa Aircraft |
Europa Classic |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After commencing take off roll and moving throttle to full ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: After commencing take off roll and moving throttle to full power, the aircraft yawed left uncommanded and rolled sharply right after lifting the tail wheel. It seems that simultaneously – the pilot cut throttle, propeller struck the runway, one blade departed, and the aircraft to a stop under control on grass 3-5 meters left of runway 09. |
4/10/2020 |
OCC2151 |
Geraldton |
WA |
Airborne |
XT 912 SST |
Rotax |
912 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Due to vibration on the wheel spat after taking off, the bra...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Due to vibration on the wheel spat after taking off, the bracket where the spat attaches to on the inside broke in half. The spat was still secure but was visibly looser.
Outcome: Information on failure supplied to aircraft manufacturer. Aircraft owners are reminded to carry out a thorough preflight inspection in accordance with the Pilots Operating Handbook for their aircraft Make/ Model |
3/10/2020 |
OCC2177 |
Ararat Aerodrome |
VIC |
Arion |
Lightning |
Jabiru |
3300A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: While conducting a landing at an aerodrome, the aircraft stru...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: While conducting a landing at an aerodrome, the aircraft struck light fixtures to the side of the runway and hit a fence. The pilot noted possible confusion within the cockpit resulted in the throttle being reduced to idle during the go-around. The accident was not reported within the required 72 hour timeframe.
RAAus reminds members of the importance of clear communication by the pilot when carrying passengers and the requirement under Section 4.08 of the RAAus Flight Operations Manual to report all accidents and incidents to RAAus which fulfils the reporting requirements under the Transport Safety Investigation Act (2003) for the Australian Transport Safety Bureau requirements. |
2/10/2020 |
OCC2141 |
Gawler Airfield |
SA |
Jabiru |
J 170C |
Jabiru |
Gen 3 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was on climb out after take-off when there was a...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was on climb out after take-off when there was a severe vibration. The aircraft landed safely and on inspection it was found that the leading edge of a propellor blade was missing. |
1/10/2020 |
OCC2157 |
Kapunda |
SA |
Jabiru |
J230-D |
Jabiru |
3300 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After having maintenance completed on the aircraft, the pilo...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: After having maintenance completed on the aircraft, the pilot conducted two touch and goes before departing to ensure everything was running smoothly. Everything was fine on the two touch and goes so the pilot departed the field and started tracking for YCVA. Roughly 42 NM into the flight 0.4hrs the pilot started to smell a burning smell from the aircraft. It was at this point they powered back slightly and the smell went away. Shortly after this they noticed the aircraft was losing oil pressure rather quickly and they noticed the burning smell again. The pilot immediately started looking around for places to land and realised they were about 8NM from a friends’ airfield and decided to land there.
The pilot landed with no issues and taxied up to the front of the hangar. They exited the aircraft to find oil sprayed all over the left hand side of it, from the nose wheel the whole way along the belly and main wheels to the elevator. The cowling was removed to see where the oil was coming from. At first it was not clear as there was a lot of oil spread around. The pilot then rang the maintainer to tell them the plane was covered in oil, the burning smell and that the oil pressure dropped during the flight. The maintainer advised the pilot to return so they could look what was wrong. During the call the oil was found to be coming out of the rocker oil tube. The pilot told the maintainer that the rocker oil tube is visibly loose and oil was definitely coming out of it. The maintainer then replied that they forgot to do up the rocker oil tube. They then instructed the pilot how to do up the rocker oil tube, replace the oil. (they had 2x w100 piston engine oil bottles with them). After the pilot did this and cleaned the oil off the aircraft they completed a successful engine run up on the ground. They then flew directly back to Jamestown rather than stopping at Clare valley as originally planned. The flight back to Jamestown was uneventful and once landed, rechecked the oil and it was still at an appropriate level. |
1/10/2020 |
OCC2142 |
Warwick Aerodrome |
QLD |
Jabiru |
J 230 C |
Jabiru |
3300 A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Complete engine failure with seizure whilst cruising at 3,500...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Complete engine failure with seizure whilst cruising at 3,500 feet AGL.
Determined Outcome: Failure of No.4 piston/gudgeon pin. |
29/9/2020 |
OCC2133 |
Tongala |
VIC |
Kappa |
KP-5 ASA |
Rotax |
914UL2 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The landing gear failed to lock down resulting in a gear up ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The landing gear failed to lock down resulting in a gear up landing. Further review identified that the actuator had delatched. The aircraft was repaired and returned to service. |
28/9/2020 |
OCC2116 |
Ballarat Aerodrome |
VIC |
Tecnam |
Sierra |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Following pre-take off checks in the run-up bay to Runway 36...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Following pre-take off checks in the run-up bay to Runway 36, the pilot lined up for take-off after touchdown of another aircraft, which landed long and proceeded to taxi to the runway exit point (which is the cross-strip 05/23). The pilot had clear forward sight of the other aircraft and upon seeing it commence its turn onto Runway 23 but did not waiting for a "clear-of-duty-runway" radio call. The pilot judged that it was safe for them to depart and gave their "rolling" call and commenced take-off.
For the future, the pilot will ensure a call advising clear of runways is received and will confirm the runway is clear before proceeding. |
27/9/2020 |
OCC2134 |
Bendigo Aerodrome |
VIC |
Tecnam |
P92 Eaglet |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: At a busy aerodrome and during dual circuit training for an h...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: At a busy aerodrome and during dual circuit training for an hour the student had been making consistent Downwind and Base radio calls. The circuit traffic was constantly more than one aircraft. Two-way radio communication had been confirmed as fully operational at the beginning of the training session. The preceding circuit before the proximity incident an inbound call was heard from a VH registered aircraft inbound from the south west. The reporting Tecnam was airborne of runway 17 with a second Tecnam on crosswind for RWY 17. A third Tecnam was to the west of the field.
Due to possible radio congestion, high workload for the pilots and differences in circuit sizes, the VH registered aircraft and one of the Tecnams were reported as moving into close proximity. Members are reminded of the need to maintain situational awareness, keep radio calls to that relevant for alerted see and avoid and as required under CAR166C. |
27/9/2020 |
OCC2129 |
Bendigo Aerodrome |
VIC |
Arion |
Lightning |
Jabiru |
3300 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Aircraft was powered up to normal power for take-off on RWY17...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Aircraft was powered up to normal power for take-off on RWY17. As the aircraft rotated began to climb, a couple of small stutters in the engine was noticed. Power was throttled back and the aircraft was landed back down onto the remaining runway without incident. On leaving the runway at the end of the runway, the engine stopped. The engine was started again and it fired up immediately, however was running rough and stopped again at which point it was decided not to attempt restart and instead tow the aircraft to the apron. Review identified the cause likely due to vapour lock. |
27/9/2020 |
OCC2128 |
Archerfield Aerodrome |
QLD |
Aeropro |
3K Eurofox |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst conducting circuits with a student under dual instruct...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst conducting circuits with a student under dual instruction, the student performed an uneventful take-off on runway 28R. At approx. 600ft AGL on crosswind, the instructor noticed the engine was not performing entirely consistently, with intermittent power loss. The instructor turned the aircraft back toward the direction of the airport as a precaution and took the throttle. They partially cycled the throttle back to full throttle however did not regain full performance from the engine. The instructor declared MAYDAY to the control tower, who cleared the aircraft to land on all available runways. The aircraft landed uneventfully. Review identified power loss occurred due to fuel starvation caused by fuel vapour lock. |
27/9/2020 |
OCC2138 |
Bankstown Aerodrome |
NSW |
Aeroprakt |
A22LS Foxbat |
Rotax |
912Uls |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: When initially starting the engine the fuel valves were clo...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: When initially starting the engine the fuel valves were closed and the engine stopped after 30 seconds. The pilot restarted the engine with the right tank open and the engine started as normal. Whilst completing circuits with a student and on take-off on upwind, the engine started vibrating with the Rpm coming down to about 3000 rpm. The instructor initiated a turn back to land on the same runway (29L) in the opposite direction (11R) alerting tower. Tower cleared the aircraft to land which it did uneventfully. |