Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
19/10/2017 |
OCC1188 |
Various |
VIC |
Super Petrel |
Sea Plane |
Rotax |
912 ULS |
Possible Multiple Airspace Incursions
DETERMINED OUTCOME: Member had cross country certificate su...
|
Possible Multiple Airspace Incursions
DETERMINED OUTCOME: Member had cross country certificate suspended. Member has undergone retraining and successfully regain a cross country certificate. |
18/10/2017 |
OCC1177 |
1nm N of Mount Cotton |
QLD |
EuroFox |
3K |
Rotax |
912 ULS |
An instructor was conducting Stalls with a student in the Eastern Training Area, and believed to be ...
|
An instructor was conducting Stalls with a student in the Eastern Training Area, and believed to be in correct area up to 3500ft. Upon their return to Archerfield they were advised that they had infringed CTA.
Outcome: The pilot has indicated their acceptance of this mistake and learnt from it. No further action required from RAAus. It is essential that members report airspace infringements (AI) to RAAus no matter the severity. These incidents allow RAAus Safety to analyse AIs at a national level and communicate with AirServices Australia and the Military regarding airspace violations, improvements and access. |
15/10/2017 |
OCC1218 |
Bajool |
QLD |
Jabiru |
J230D |
Jabiru |
3300A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The bracket that holds the brake calipers on to the l...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The bracket that holds the brake calipers on to the landing leg broke.
DETERMINED OUTCOME: This issue has been referred to the CASA Engineering and Airworthiness Branch for monitoring and action as required. The importer has also been notified. |
14/10/2017 |
OCC1169 |
Wynyard |
TAS |
Fly Synthesis |
Storch S500 |
Rotax |
912LS |
The aircraft was on the apron 30m from the Club House warming up the engine. The park brake was appl...
|
The aircraft was on the apron 30m from the Club House warming up the engine. The park brake was applied lightly and the revs were increased. The aircraft moved forward and the pilot reached to apply more brake. In doing so their right hand became entangled in the passenger seat belt. The pilot then took their left hand off the throttle to untangle their right hand, and inadvertently bumped the throttle which increased the revs dramatically. The aircraft surged forward and veered to the left. Before the pilot had time to untangle their hand the aircraft had stuck the building.
OUTCOME: No further action required by RAAus. Pilots are reminded to ensure all items are secure and that no objects will restrict on the safety operation of the aircraft. |
13/10/2017 |
OCC1197 |
Caboolture |
QLD |
Jabiru |
J170-C |
Jabiru |
2200B |
A pilot flew an aircraft without a compliant pilot certificate.
Outcome: The pilot was upfront ab...
|
A pilot flew an aircraft without a compliant pilot certificate.
Outcome: The pilot was upfront about this issue and subsequently resolved the deficiency. No further action required. |
13/10/2017 |
OCC1199 |
Caboolture |
QLD |
Jabiru |
J170C |
Jabiru |
2200B |
Unauthorised instruction of pilot.
Outcome: The pilot was upfront about this issue. No further ac...
|
Unauthorised instruction of pilot.
Outcome: The pilot was upfront about this issue. No further action required. |
11/10/2017 |
OCC1173 |
Latrobe Valley Aerodrome |
VIC |
Tecnam |
P92 Eaglet |
Rotax |
912 |
After take-off, being about 200-300 AGL, still climbing a vibration started and significant power wa...
|
After take-off, being about 200-300 AGL, still climbing a vibration started and significant power was lost. Once power was lost, the pilot set the glide attitude, doing some of the trouble checks, slipping the machine to try and get it to the runway first. Once it was obvious the aircraft wasn't going to make the runway, the pilot selected a field and landed in it.
Outcome: Some very minor wear in one of the carburetors was identified. 2 new carburetor kits were installed and the aircraft has been operating since. An inspection of the suspect carburetor identified that it had flooded causing the engine to stop but the internal wear didn't actuality appear to be the cause. No further action required. |
10/10/2017 |
OCC1208 |
Gawler Aerodrome |
SA |
Jabiru |
J170-D |
jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: During CCTs the pilot noticed an engine vibration and...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: During CCTs the pilot noticed an engine vibration and made full stop landing. An investigation revealed low compression on No 1 cylinder, further investigation revealed a cracked cylinder along a machined surface. All cylinders were replaced with replacement cylinders supplied by the manufacture which included a modification to the machined surface.
DETERMINED OUTCOME: This issue has been referred to CASA Airworthiness and Engineering section. As it is a registered LSA RAAus is limited in what it can do to resolve this issue. |
9/10/2017 |
OCC1171 |
Moorabbin |
VIC |
Aeroprakt |
A32 Vixxen |
Rotax |
912 ULS |
The pilot encountered radio failure inbound from Carrum. The pilot tried troubleshooting e.g. chang...
|
The pilot encountered radio failure inbound from Carrum. The pilot tried troubleshooting e.g. changed headsets, turned radio on/off, reduced power load and tried contacting the tower several times to no avail. The pilot then squawked 7600 and continued inbound via Carrum to RWY 17R.
Outcome: The pilot in command followed the correct procedures for radio failure. The pilots actions ensured the safety of his aircraft and other airspace users was maintained. |
8/10/2017 |
OCC1165 |
Jaspers Brush |
NSW |
Evektor |
Sportstar |
Rotax |
912 ULS |
Coming in to land on RWY24 after a 45min local area flight with in the training area. Approach was n...
|
Coming in to land on RWY24 after a 45min local area flight with in the training area. Approach was normal until short final when the pilot went to reduce power could not get the rpm below 3000. After checking the friction lock was off and throttle fine tune was fully reduced the pilot decided on a glide landing, rather than to go around and possibly have further engine issues. The pilot turned off the engine, applied full flap and landed normally, although slightly long and rolled to RWY intersection and turned off onto TWY. When restarted, the engine rpm was still at 2000 and would not go lower. The pilot taxied and hangared the aircraft, noting issue in maintenance log and reported it to aircraft owner and local maintainer.
DETERMINED OUTCOME: The aircraft has been looked at by a L2 / LAME and it appears the issue was due to wear and tear of the throttle cable. The cable has since been replaced. |
7/10/2017 |
OCC1178 |
Canberra |
ACT |
Jabiru |
J230D |
Jabiru |
3300A |
The aircraft engine surged 5 times during climb out, at approx. 3500 ASL. The pilot returned immedia...
|
The aircraft engine surged 5 times during climb out, at approx. 3500 ASL. The pilot returned immediately to Canberra airport, no further problems during remainder of the flight. The pilot ran an engine check after landing, magneto test & carby heat, all were OK. On close examination, the underside of the carburetor was found to have extensive fuel stains. New carburettor installed. No further issues identified. |
6/10/2017 |
OCC1163 |
Albany Regional Airport |
WA |
Jabiru |
J170C |
Jabiru |
2200B |
Normal take-off on RWY05. At approximately 300ft the engine suffered significant loss of power accom...
|
Normal take-off on RWY05. At approximately 300ft the engine suffered significant loss of power accompanied by vibration/rough running. With insufficient runway remaining to land, performed a gentle turn back towards the threshold of RWY14. The pilot found that with reduced throttle the engine could maintain about 1800rpm. The pilot elected to perform a tight sweeping approach back onto RWY05 (which was more into wind) rather than land downwind on 14. The landing was uneventful. Upon shutdown oil was found leaking from around the exhaust manifold #4 cylinder, the plugs on #4 cylinder were totally oiled up.
DETERMINED OUTCOME: This occurrence has been referred to CASA engineering and airworthiness branch and the manufacturer for further monitoring and action where required. It appears a valve failed. |
3/10/2017 |
OCC1166 |
Camden |
NSW |
Brumby |
R600 |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The aircraft owner reported that the seat back locati...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The aircraft owner reported that the seat back locating track had torn metal. An investigation disclosed that on pilot's side one track was pulling the anchor nuts through the floor pan. There was then distress discovered with all of the rail attachments. The floor pan and structure below the floor is of .020 material and not strong enough to take much load.
OUTCOME: This has been reported by the RAAus Technical Manager to the manufacturer and in time they will respond. The owner has also been advised to register their concerns directly with the manufacturer to ensure the issue is resolved to satisfaction. |
2/10/2017 |
OCC1164 |
Archerfield |
QLD |
The Aircraft Factory |
Sling LSA |
Rotax |
912 LS |
The aircraft suffered a loss of directional control while landing aircraft resulting in runway excur...
|
The aircraft suffered a loss of directional control while landing aircraft resulting in runway excursion.
Outcome: The pilot in command has self-remediated to address the root cause of R-LOC. |
2/10/2017 |
OCC1160 |
Chinchilla |
QLD |
Jabiru |
J230D |
Jabiru |
3300A |
The pilot maintained too much pressure with their right foot on the rudder, resulting in the aircraf...
|
The pilot maintained too much pressure with their right foot on the rudder, resulting in the aircraft veering sharply to the right and hitting a tree sustaining minor damage.
DETERMINED OUTCOME: A detailed ground based review was conducted with CFI to revise strategies for control management and authority during critical flight phases. The student training records were reviewed and prior training deficiencies discussed. The aircraft has subsequently been fully repaired by the manufacturer and returned to service. |