Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
3/1/2019 |
OCC1579 |
Moorabbin Aerodrome |
VIC |
Bristell |
NG5 |
|
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The student vacated 31L then onto Foxtrot before calling grou...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The student vacated 31L then onto Foxtrot before calling ground for the apron. They did not ask for a clearance to use 31L.
OUTCOME: This was the student's first solo flight. The student was grounded, retrained over four subsequent flights and released to flying. Since then, student has completed further 3 solo flights, with no further occurrence. |
30/12/2018 |
OCC1572 |
Wynyard Airport |
TAS |
Aeroprakt |
A22LS Foxbat |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Defect: Copper break line of the Foxbat A22LS fractured at a ...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Defect: Copper break line of the Foxbat A22LS fractured at a bend radius due to fatigue whilst putting the park brake on at rest. Defect reported to manufacturer. |
29/12/2018 |
OCC1566 |
Bankstown Aerodrome |
NSW |
Aeroprakt |
A22LS |
|
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During pre-flight procedures the student had the fuel caps l...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: During pre-flight procedures the student had the fuel caps loosened, waiting for the aircraft to be refuelled. The instructor decided there was enough fuel onboard to continue with the sortie and the pair departed. Whilst in the run-up bay the fuel caps fell off. The aircraft proceeded to take off while the company found the fuel caps on the ground. The aircraft returned to land without issue.
The Instructor did not double check the fuel caps were tightened and student tried to help the refueller by leaving fuel caps loose. In future, the instructor will be vigilant to conduct pre-flight checks after student has done so. |
24/12/2018 |
OCC1563 |
Bankstown training Area |
NSW |
AEROPRAKT |
22-ls |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Stalls and practice forced landings were being conducted in t...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Stalls and practice forced landings were being conducted in the Bankstown training area near Camden airport. The engine started running rough and the PIC made the decision was made to return to Camden airport for a Full stop landing. Reporter stated that they suspected water in the fuel was the causal factor as the aircraft had been washed directly prior to flight. Abnormal pitch and roll attitudes during stalls and simulated engine failures could possibly send water ( heavier than fuel) to the fuel tank sump intermittently. |
24/12/2018 |
OCC1567 |
at above address - Pacific Haven Airpark |
QLD |
Jabiru |
J200-B |
Jabiru |
J 200 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: A 'kink' developed in fuel line resulting in fuel sta...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: A 'kink' developed in fuel line resulting in fuel starvation on takeoff. A new fuel filter had been tested, installed and engine run-up performed on ground to test, which indicated normal operations. However, on take-off at approximately 50 feet AGL engine noticeably dropped revs. The pilot conducted a landing by closing the throttle, lowering the nose and selecting full flap on remaining 500 metres and taxied back to the hangar.
The new filter had been connected without noticing that the fuel line at the electric pump end had kinked due to it being enclosed in the center console and therefore not being visible. The new filter was marginally larger than the old one. Some fuel was getting through but not enough to satisfy normal takeoff requirements.
The pilot elected to shorted the fuel line from electric fuel pump to fuel filter by approximately 10mm thus straightening line and removing the kink. After conducting fuel flow tests the unit proceeded to producing maximum flow. |
22/12/2018 |
OCC1562 |
Sunshine Coast Aerodrome |
QLD |
Sling 2 |
Sling 2 LSA |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Student was conducting circuits outside of tower hours as CTA...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Student was conducting circuits outside of tower hours as CTAF operations and came in a little faster than usual in an effort to avoid a Jetstar A320 departing shortly. Due to excessive airspeed during the approach and flare the student touched down hard with a higher than usual airspeed. This resulted in a large bounce, with incorrect recovery technique, pushing the control stick forward and pitching down. The aircraft pitched down very steeply with a high rate of descent and impacted the runway on the nose wheel which collapsed. OUTCOME: The student will undertake remedial training. |
20/12/2018 |
OCC1980 |
Gilgandra |
NSW |
Arion |
Lightning |
Jabiru |
3300 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst flying from Redcliffe QLD to Narromine NSW tracking vi...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst flying from Redcliffe QLD to Narromine NSW tracking via Gatton and Wee Waa, the aircraft was on autopilot for most of the flight. Conditions were hazy even close to Brisbane. Beyond Warwick the pilot couldn’t discern a distinct horizon, however abeam Moree they could still see the large grain silos next to the airport from 25km away. As the aircraft got to Wee Waa it became progressively hazier. Visibility over the engine cowl was negligible and to maintain a sense of the aircraft’s attitude required looking at ground features to the side of the aircraft. Abeam Gilgandra at 4,500’ it quickly got worse – almost like the aircraft flew into a denser cloud of dust within the thickening haze. At this point the pilot couldn’t see Gilgandra airstrip about 7km out to their left - and then lost sight of the ground. This was a scary moment and being on autopilot didn’t allay the pilots’ fears as much as you would probably expect. The pilot could only stare at the artificial horizon on the EFIS while they cancelled Altitude Hold on the autopilot, throttled back and descended. Within 30 seconds or so they started to regain visual attitude references, and flew the remaining short distance under clearing conditions to Narromine at 2,500’.
The loss of visibility was due to smoke from farmers burning off. |
20/12/2018 |
OCC1620 |
Taree Aerodrome |
NSW |
Hornet |
Hornet |
Rotax |
914 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: While conducting circuits the aircraft radio failed. The pilo...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: While conducting circuits the aircraft radio failed. The pilot wasn't aware of the failure until another aircraft came in to land. As soon as the pilot became aware of the problem he landed and ceased flying. The radio failure was identified as a wiring issue in the PTT and was rectified.
RAAus reminds pilots of their obligation to ensure the radio of an aircraft is operational and functioning correctly as part of serviceability checks prior to aircraft movement. |
19/12/2018 |
OCC1560 |
Mildura Aerodrome |
VIC |
Fantasy Air |
Allegro |
Rotax |
912 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: While taxiing at a busy airport with scheduled passenger flig...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: While taxiing at a busy airport with scheduled passenger flights, the pilot inadvertently taxied between a passenger aircraft and the terminal, causing safety concerns for passengers.
The pilot received remedial training and provided a formal apology to the airport operator and passenger airline.
Pilots are reminded to ensure they are familiar with the airport ground taxiways markings and consider the safety of uninformed participants when operating at unfamiliar airports. |
19/12/2018 |
OCC1571 |
Bribie island |
QLD |
Storch aviation |
Slepcev Storch ss4 |
Rotax |
912s |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Departing from Donnybrook, the pilot encountered carburetor i...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Departing from Donnybrook, the pilot encountered carburetor icing and elected to conduct a precautionary landing on Bribie Island. Once the aircraft was safely on the ground, an assessment of the engine was conducted and the pilot departed with no further icing. |
19/12/2018 |
OCC1565 |
Port Pirie Aerodrome |
SA |
Zenith |
Zodiac CH 601 XL-B |
Honda |
Viking 110HP |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: While in cruise the battery voltage was noticed to be droppin...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: While in cruise the battery voltage was noticed to be dropping at a constant rate from 13.8V. A diversion was made to the nearest aerodrome and all non-essential electrical systems were turned off.
The alternator was replaced with a 50A unit (original was 40A) of the same size and weight as all electric systems were found to be using approx 38A. The excitation wiring was replaced. Flight testing showed a constant 13.8V charge. No further abnormal indications present. |
18/12/2018 |
OCC1555 |
Bankstown Aerodrome |
NSW |
BRM Aero |
Bristell NG5 |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During circuit training the student inadvertently pressed the...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During circuit training the student inadvertently pressed the frequency quick-change button on the control stick. The instructor didn't notice that the aircraft was now monitoring the Ground/SMC frequency. On downwind the student attempted to do his downwind report on the ground frequency and was subsequently informed that was the case. Instructor returned the frequency to the Tower frequency and as an added measure set the COM 2 to monitor the tower frequency as well in case it happened again. |
17/12/2018 |
OCC1554 |
Sydney training area |
NSW |
Aeroprakt |
A22LS Foxbat |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The instructor conducted a flight training sortie with a stud...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The instructor conducted a flight training sortie with a student in the northern end of the Sydney training area approximately 6-7nm west of Warragamba Dam. At approximately 4000ft the instructor simulated an engine failure by reducing the throttle to idle for the student to conduct a Practice Forced Landing (PFL). The student had conducted a successful PFL and at about 800ft AMSL applied power in the process of the climb out. At about 1200ft AMSL the aircraft experienced abnormal engine indications resulting in an uneventful forced landing. Nil defects evident on groud. Potential vapour lock. |
17/12/2018 |
OCC1553 |
Cessnock Aerodrome |
NSW |
Arion |
Lightning |
CAMit |
3300SLRE |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: While on final approach to runway 35 at Cessnock, a go-around...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: While on final approach to runway 35 at Cessnock, a go-around was initiated due to an aircraft conducting low level circuits, appearing on the runway ahead of the RAAus aircraft. When the throttle was advanced to conduct the go-around, the aircraft engine began to run roughly. Climb out was impossible and the plane was landed in the last 400 metres of the runway without incident. At this stage the other aircraft was stationary in the middle of the runway about half way down the strip. Examination of the engine has not yet revealed a cause for the rough running but the problem is reproducible on the ground and still being investigated. |
13/12/2018 |
OCC1557 |
Sunshine Coast Aerodrome |
QLD |
The Airplane Factory |
SLG2 |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Aircraft entered airspace from incorrect waypoint as clearanc...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Aircraft entered airspace from incorrect waypoint as clearance was to proceed northbound west of the motorway. Instead, the aircraft crossed to the eastern side of motorway 1nm before clearing YBSU airspace. The instructor had been distracted, focussing on student patter. The instructor has acknowledged and determined that future patter should be restricted when operating during critical phases of flight. |