Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
15/1/2022 |
OCC2684 |
Port Macquarie Aerodrome |
NSW |
Sonex |
Sonex |
Jabiru |
3300A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft experienced an engine failure after take off. Fu...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft experienced an engine failure after take off. Further inspection revealed that the occurrence was as a result of the flywheel bolts which had become loose. |
14/1/2022 |
OCC2915 |
Gympie Aerodrome |
QLD |
Aeroprakt |
A22LS Foxbat |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The upper engine cowling fastener was not secured and the c...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The upper engine cowling fastener was not secured and the cowling flexed while in flight, impacting the boss of the propellor. This occurred at 500ft AGL on initial climb out, during a training flight. The SI took over and the aircraft was landed safely.
Subsequent review indicated the standard process was for the pilot to slide a hand inside the air vent to support the bottom cowling which ensured the fastener was secured in the catch. |
13/1/2022 |
OCC2682 |
Tyabb Aerodrome |
VIC |
Aeroprakt |
A22LS Foxbat |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During dual instructional touch and goes, the student lost di...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During dual instructional touch and goes, the student lost directional control, first to the left then to the right. The instructor took over however, couldn’t recover the directional control. When the instructor realised it would not climb they reduced power to idle and brought the aircraft into the paddock to the right, it cartwheeled once on touching down in the paddock and came to a halt on its roof, upside down. |
13/1/2022 |
OCC2681 |
Lismore |
NSW |
Jabiru |
J-170C |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a dual flight with a student, a taxi call (with intent...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a dual flight with a student, a taxi call (with intentions to depart to the SW) and entering back-tracking call were made for runway 15 at Lismore. Shortly after take-off on runway 15, (passing through approx. 300-400ft AGL) an inbound call was heard from a Foxbat aircraft, stating they were inbound from the south-west at 1000ft. Believing no conflict existed, the training aircraft continued climbing on runway heading (150 degrees) with intentions to reach 1500ft and/or 3nm prior to departing from upwind to the south-west by a right turn. Upon reaching 3nm from Lismore, passing through 1300ft, a departure call was made stating they were "departing off upwind runway 15, passing through 1300ft, on climb to 1500ft and shortly tracking to the south-west". Shortly after this call, and passing 1400ft, the start of another radio call was heard from the Foxbat, prior to the training aircraft seeing the Foxbat directly ahead and below the nose, breaking off into a right hand turn to avoid them. It is estimated there was approximately 300-400ft vertical separation (based on the Foxbat reporting inbound at 1000ft), and the Foxbat passed down the left side and below. No collision or damage occurred.
Pilots are reminded of the critical importance of alerted see and avoid and for broadcasts to contain accurate position and height information, particularly at busy non-controlled airports. |
12/1/2022 |
OCC2680 |
Caboolture |
QLD |
Rainbow SkyReach |
Cheetah XLS (Bushcat) |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During pre-flight it was noted that where the elevator cable...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During pre-flight it was noted that where the elevator cable exits the empennage near the horizontal stabilizer, the aircraft skin has rubbed the protective coating from the cable exposing the strands. Nil strands damaged at this stage |
11/1/2022 |
OCC2683 |
Launceston Aerodrome |
TAS |
Jabiru |
J160C |
Jabiru |
Gen 4 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Carbon monoxide (CO) was indicated in the cockpit. The aircra...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Carbon monoxide (CO) was indicated in the cockpit. The aircraft was fitted with a card CO detector on the instrument panel which was noticed by the flight crew to discolour. A crew member experience symptoms consistent with elevated levels of CO exposure. There was no report of any new act intervening which might cause an abnormal presence of CO in the cockpit and there was no previous history of CO ingress into the cockpit. Further inspection revealed that a missing rear fairing screw was allowing carbon monoxide to enter the cockpit. The screw was replaced and issue resolved. Pilots and aircraft owners are reminded that the presence of carbon monoxide within the cockpit may result in pilot/passenger incapacitation. Fitment of electronic carbon monoxide detectors are strongly recommended and available from the RAAus shop. More information on the dangers of carbon monoxide are available from the ATSB and CASA websites. |
11/1/2022 |
OCC2776 |
Caboolture |
QLD |
Tecnam |
P92 Echo S |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The lower longerons for the aircraft frame showed signs of co...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The lower longerons for the aircraft frame showed signs of corrosion |
10/1/2022 |
OCC2677 |
Bendigo Aerodrome |
VIC |
Jabiru |
SP500 |
Jabiru |
3300 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The Jabiru was taxiing for departure from runway 36. There we...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The Jabiru was taxiing for departure from runway 36. There were three other aircraft in vicinity. A twin aircraft was lined up runway 36, a Cessna 172 just landed and exiting, another Cessna 172 in run up bay. It took approx. 6-7mins to taxi to holding point on runway 35. The Jabiru pilot had confirmed their radio was working as they had asked the Cessna how much longer before they would be departing. There had been no other calls on frequency. The Jabiru pilot called entering 35 for departure to the east. As they lined up a twin aircraft overflew and went around. The twin aircraft must have been on short final when the Jabiru entered runway. The Jabiru pilot didn’t see them, and they didn’t call the Jabiru when it entered and they saw there was going to be a conflict. The Jabiru departed without further incident.
Pilots are reminded of the critical need for alerted see and avoid, particularly at busy non-controlled airports |
9/1/2022 |
OCC2678 |
Remlap Park Allworth |
NSW |
FPNA |
A22 Valor |
Rotax |
912 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft experienced a hard landing due to wind shear. Th...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft experienced a hard landing due to wind shear. The pilot completed a go around and on the second landing the aircraft went to the left due to a damaged nose wheel. There was also damage to the propellor and RH wing as the nose wheel collapsed. |
2/1/2022 |
OCC2672 |
Shellharbour Aerodrome |
NSW |
Evektor |
SportStar Plus |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a gusty crosswind landing, the right wingtip contacted...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a gusty crosswind landing, the right wingtip contacted the ground, resulting in damage to the right wing. The pilot will complete revision of crosswind management techniques prior to flight in crosswinds and was unfamiliar with the aircraft type. |
30/12/2021 |
OCC2746 |
Tocumwal |
VIC |
BRM Aero |
Bristell S-LSA |
Rotax |
912 ULS 2 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During flight on return to Yarrawonga from Echuca the engine...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During flight on return to Yarrawonga from Echuca the engine began losing power and running rough, coin-sided with an erratic CHT reading. The pilot had been able to reduce power to idle which allowed the engine to begin running smoothly again. After a short period of time after the power had been advanced back to around 60% percent to keep the engine running smooth and CHT indication to be within normal range. This process had been repeated with four separate occasions of the engine running rough. The pilot had contacted Melbourne centre after the second occurrence and planned a diversion to Tocumwal where they made a safe landing. |
30/12/2021 |
OCC2671 |
Goolwa Aerodrome |
SA |
Jabiru |
J230 - C |
Jabiru |
3300A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft took off, completed three circuits and departed...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft took off, completed three circuits and departed the circuit area for flight over Hindmarsh Island to Murray Mouth then returned overhead Clayton. The pilot joined mid downwind 01, completed downwind checks, landed long due to the rough surface of the runway but had fully landed and deployed brakes when they lost control and veered from the end of the runway.
The aircraft collided with the rear of a hangar as well as a water tank and the door support of a second hangar. The pilot tried to avoid the collision by firstly applying power to power out of the situation but there was not enough lift available, so they applied brakes again and aimed as well as they could for the gap between a water tank and the door support of a hangar, such that the wings would take the brunt of the force. The aircraft continued on and came to rest in the rear wall of a hangar. The pilot switched of the Master switch but could not switch off fuel due to ruptured fuel tanks. The passenger and pilot were able to exit the aircraft via the right hand door and leave the hangar via a damaged wall panel.
The pilot noted a wind change had been forecast (to become a tailwind on 01) and believes this had just occurred as they touched down.
Subsequent discussion with the pilot revealed they realised they could have landed shorter, could have conducted an orbit to allow the wind change to establish and then repositioned for the other direction. |
30/12/2021 |
OCC2670 |
Maitland Aerodrome |
NSW |
Czech Sport Aircraft |
Piper Sport |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The nose wheel collapsed on an aborted take-off when the cano...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The nose wheel collapsed on an aborted take-off when the canopy opened due to not being re-latched after pilot distraction. |
29/12/2021 |
OCC2667 |
Boonah Aerodrome |
QLD |
Tecnam |
P96 Golf |
Rotax |
912ULS |
Shortly after a normal touchdown the right undercarriage leg sheared off at the undercarriage bracke...
|
Shortly after a normal touchdown the right undercarriage leg sheared off at the undercarriage bracket. |
27/12/2021 |
OCC2666 |
Ballina Byron Gateway Aerodrome |
NSW |
ICP |
Savannah VG |
Rotax |
912-ULS3 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: When the aircraft was ready to depart YBNA the pilot gave a ...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: When the aircraft was ready to depart YBNA the pilot gave a taxi call to BN CTR and was advised to hold as an RPT was inbound. The pilot held till aircraft had landed and cleared runway and then gave back tracking and rolling call. As the aircraft reached about 700 feet and tracking for the beach the pilot had a call from BN CTR requesting their track and altitude. The pilot advised that they were tracking north along the beach not above 1000ft. BN CTR then called again with the same request. The pilot repeated the advice but BN CTR said it was unreadable. The pilot continued on their track north along the beach and the received a call from BN CTR saying they had aircraft tracking to YBNA and requested them to land ASAP as they did not know their location. The pilot looked for landing site and saw they were abeam YTGH so immediately landed there. When on the ground they looked up a phone number for BN CTR and called them. After explaining why they were calling they were redirected to another number and was told someone would call back. Some 5mins later a call came from operations and the pilot explained what had happened and where they were. The pilot was advised not to proceed with the flight until they had their radio problem fixed. A technician was working at YTGH and they were able to check the radio equipment. It turned out that the microphone on the headset had a worn wire which was intermittently working. The pilot checked out another headset which was working and so was able to proceed with the flight which was completed uneventfully. |