Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
12/9/2023 |
OCC3421 |
Yarram Aerodrome |
VIC |
Fly Synthesis |
Texan TC |
|
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was on an approach to Runway 09 at Yarram Airport. ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was on an approach to Runway 09 at Yarram Airport. They misinterpreted the wind as blowing from the west when it was in fact blowing from the east, they were focusing on traffic in the area. The pilot made an approach to Runway 09. During the landing they realized something was wrong and attempted to go around however, the aircraft wasn’t able to climb. They landed again and applied full braking, however, were running out of runway. They applied full left rudder too avoid departing the end of the runway. The aircraft went into the grass adjacent the runway where the nose landing gear collapsed and the prop struck the ground. |
6/9/2023 |
OCC3426 |
Tamworth Aerodrome |
NSW |
Tecnam |
P2004B |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Taking off on 30L for the first lesson of circuits for the da...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Taking off on 30L for the first lesson of circuits for the day, during a full power climb to circuit height, just prior to reaching that altitude both the pilot in command and the student under instruction (aircraft owner) noticed an abnormal vibration coming from the engine. Upon power reduction during level off to cruise power the vibration stopped.
This aircraft issue was that it had a sunken fuel bowl float. |
6/9/2023 |
OCC3406 |
Caloundra Aerodrome |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was conducting circuit practice on runway 30 at Cal...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot was conducting circuit practice on runway 30 at Caloundra. On the second circuit and touch and go they landed hard then bounced and was slow to initiate a go around the aircraft pitched forward and nose wheel hit runway abruptly then snapped and prop struck the runway. The aircraft slid for ten meters then come to a stop on the runway. The pilot turned everything off and exited the aircraft. |
2/9/2023 |
OCC3422 |
Innisfail Aerodrome |
QLD |
Pipistrel |
Alpha |
Rotax |
912 UL2 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Student was cleared for their first solo circuit and made a n...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Student was cleared for their first solo circuit and made a normal approach to runway 14, upon flaring the PIC bounced the aircraft and elected not to go round as previously briefed, but landed a second time heavily causing a partial failure of the right undercarriage leg. The aircraft then veered off the runway onto the grass and completed a half-ground loop coming to rest. |
27/8/2023 |
OCC3447 |
Caboolture |
QLD |
Skyreach |
Bushcat |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The LSA Bushcat Rotax fuel pump drainage hose is routed, by d...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The LSA Bushcat Rotax fuel pump drainage hose is routed, by design, to protrude directly into the slipstream on the port side of the aircraft. This design and installation appears to be in direct contradiction to instructions in the Rotax Installation Manual. The manufacturer, Skyreach, was notified of the issue in August 2023.
BRP Installation Manual Section 73-00-00. Observe correct routing of drainage line. Drainage line have to be routed into a ram-air and vacuum free zone, according to the requirements and release of BRP-Rotax. The drainage line must not be routed into the slipstream. Ram pressure or vacuum impair the fuel pressure. |
26/8/2023 |
OCC3399 |
Ballina Byron Bay Gateway Aerodrome |
NSW |
Storch Aviation |
Slepcev Storch SS4 |
Rotax |
914 UL |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The following detail are provided by the ARO on duty at the t...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The following detail are provided by the ARO on duty at the time of the occurrence and the subsequent conversation with the pilot.
A Storch aircraft had two landings on the grass, when the ARO spoke to the pilot they weren’t aware they couldn’t do it and they acknowledge it was in the ERSA but their tires were worth $5k each and the bitumen ruins them. The ARO also stated with the AGL works going on there were survey pegs, pits etc all within the strip that weren’t normally there. |
26/8/2023 |
OCC3491 |
Dumgree |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912iS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot noted that the oil temperature gauge was rising and...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot noted that the oil temperature gauge was rising and due to the nearby terrain elected to perform an out landing in an open paddock.
The aircraft was found to have had a faulty oil thermostat that when it failed actually closed. This is not the normal as when they fail they stay open but in this case it closed. The aircraft has been assessed and has had been operating since with nil defect evident |
26/8/2023 |
OCC3400 |
Sunshine Coast Aerodrome |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Two slings were flying in company ferrying the aircraft to Ca...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Two slings were flying in company ferrying the aircraft to Caboolture for maintenance. At approx. 10am local time the first Sling obtained a taxi and airways clearance direct and in the readback confirmed their clearance to taxi to the holding bay A2 behind company aircraft. Unfortunately, the pilot of the second Sling erroneously understood the company aircraft to be a reference to themself and proceeded to taxi as number 2 to the first Sling to the holding point.
Being behind the first Sling, the pilot was unaware the second Sling was taxiing and consequently unable to highlight the error prior to it departing the apron onto the taxiway. ATC contacted the second Sling and advised a clearance wasn't supplied for taxi and subsequently provided a taxiway and airways clearance. The pilot of the second Sling apologised for the error and advised their assumption, given they'd heard the clearance included company aircraft, that they were indeed the company aircraft unaware a third Sling remained in the A2 holding bay. |
25/8/2023 |
OCC3394 |
Bathurst Aerodrome |
NSW |
BRM Aero |
Bristell S-LSA |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst conducting dual circuit training in a Bristell on Run...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Whilst conducting dual circuit training in a Bristell on Runway 17 in the Bathurst circuit area. A VH registered aircraft arrived and joined the circuit behind them. The student called base runway 17 for a touch and go. The VH aircraft then turned base behind them as they were turning final. The instructor made a radio call directly to the VH aircraft telling them the Bristell was at their 1 o'clock slightly low because they were close, but separation was still being maintained at this time. They acknowledged the radio call and said they would give way to the Bristell. The Bristell continued, conducted a touch and go and the instructor made a rolling call on the radio. Immediately after they made the rolling call the VH aircraft made a going around call. The Bristell conducted a slight left hand turn to spot the traffic. They saw how close they were and the instructor took over and initiated an immediate left hand turn with a radio call at approximately 150ft AGL. The VH aircraft continued with their missed approach maintaining runway heading with no adjustments to track to avoid the Bristell. Considering the runway length, the Bristell made their low level turn overhead the hangars and apron at Bathurst and they were closer to the Bristell than the intersection for RW26/08. The instructor believes this was less than 1km. As this occurrence involves a VH-registered aircraft, this has been forwarded to CASA for review. |
25/8/2023 |
OCC3393 |
Caboolture |
QLD |
Aeropro |
Eurofox 3K |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During scheduled maintenance it was noted that the oil hose f...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: During scheduled maintenance it was noted that the oil hose from the oil pump to the oil tank had shifted and the fire sleeve displayed heat damage. During replacement of the fire sleeve, heat damage of the oil hose was evident. The hose was stiff and upon flexing the hose cracked. Another hose was found stiff and brittle underneath the fire sleeve and it was also replaced. This aircraft was recently acquired and the aircraft records show the current engine was installed by another maintainer in 2021, however one of the hoses shows a date stamp of 2008. |
23/8/2023 |
OCC3392 |
Heck Field Aerodrome |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912ULS |
The PIC was conducting circuits and came in too low and slow. slight wind shear, and the left wing c...
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The PIC was conducting circuits and came in too low and slow. slight wind shear, and the left wing clipped the tree which sent the aircraft veering off to the left just before it was about to touch down. The pilot pushed the right rudder to try and straighten the aircraft but once it touched down it just kept heading left into the reeds and water on the left side of the runway. PIC subsequently conducted remedial training with a local CFI. |
22/8/2023 |
OCC3390 |
Caloundra |
QLD |
Tecnam |
P92 Eaglet |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The flight was a dual flight, conducting an Instructor renewa...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The flight was a dual flight, conducting an Instructor renewal. During a simulated practice forced landing, the pilot trimmed the aeroplane to full back trim, to set trim for the glide. At the completion of the forced landing exercise, a go-around was conducted, and the pilot attempted to trim the aircraft nose down, to relieve control loads. At this time, it became apparent that the trim was not responding to commands and stuck in the full nose-up trim position. This failure resulted in substantial control loads on the pilot to fly the aircraft at even slow speed straight and level. The resulting control loads were sufficient to require input/relief from the Examiner to assist the pilot flying in managing the control loads. The Examiner believes it would be hazardous if this occurrence had occurred with one pilot on board, particularly someone of low experience or a student solo.
They were able to safely control the aircraft and return to land at Caloundra without incident or damage to the aircraft. The L4 maintainer has inspected and uninstalled the trim actuator, finding it to contain significant water trapped in the casing, immersing electrical components. The maintainer discovered that the actuator was mechanically stuck locked in the full back position. The trim gear was stripped, likely from attempts to trim after the trim became stuck. The L4 suspects that the electric trim travel limit switch at the nose-up trim end had failed, resulting in the actuator proceeding past the limit during a trim nose-up input from the pilot, and the screw becoming jammed against the hard plastic stop at full nose-up trim position. The maintainer also believes the failure of the electric trim travel limit switch may have been caused by the water present in the unit. This defect was rectified with a replacement trim actuator unit.
It is their belief that this failed limit switch condition may have existed as a latent threat for a time before the incident, but hadn't resulted in stuck trim until a situation in which a pilot trimmed to full trim travel.
The engineer suggested to check these units internally during regular maintenance for trapped water content. Check functionality of trim to limits during pre-flight inspection. This has been forwarded back to the manufacturer as a suggestion for inclusion into the maintenance manual. |
22/8/2023 |
OCC3397 |
Shellharbour Aerodrome |
NSW |
Evektor |
Harmony |
Rotax |
912 iS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: While climbing out after take-off, passing 500 feet, a sharp ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: While climbing out after take-off, passing 500 feet, a sharp burning smell was noticed. The pilot looked around the cockpit and noticed a small amount of smoke come in through the vent on the passenger side. The pilot opened the exterior vent to allow fresh air to enter the cockpit. There was no further smoke, and the smell dissipated. The pilot returned to the airfield and the landing was uneventful.
OUTCOME: The incident was caused by one side of the scat hose becoming detached during flight and subsequently resting up against the exhaust. This has caused the scat tube to begin to smoulder. The detachment was caused by either the hose being improperly secured or through general wear and tear, resulting in the hose breaking loose from the attachment point. No non-compliances were found in relation to the pilot, aircraft or maintenance personal in relation to this incident. |
20/8/2023 |
OCC3402 |
Temora Aerodrome |
NSW |
Tecnam |
P2002 Sierra |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After landing from a local flight, a rhythmic clunking noise ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: After landing from a local flight, a rhythmic clunking noise was heard whilst taxiing the aircraft which corresponded to the taxi speed. On return to the hangar, it was identified that a brake disc retaining bolt had worked loose on the right side and was impacting the internal brake caliper section.
A replacement bolt was installed and the aircraft put away. The next time the aircraft was taxied out, it was noticed that the aircraft was pulling left. After returning to the hangar it was identified the brake piston was affected by the replacement bolt and the right brake was locked on.
OUTCOME: Aircraft brake repaired to standard using the correct bolt with no further issues identified. Member will also continue to monitor this area of the undercarriage more regularly to help eliminate future problems. |
20/8/2023 |
OCC3396 |
Coffs Harbour Aerodrome |
NSW |
Aeroprakt |
A32 Vixxen |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: A Vixxen and a Sting were in circuits on 21 making necessary ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: A Vixxen and a Sting were in circuits on 21 making necessary CTAF calls. Another aircraft (VH registered) was taxiing for 21. The VH aircraft acknowledged that they had heard both aircraft and stated their intention to use 21 to head north. As Vixxen was on final, approaching the threshold, the VH aircraft entered the runway and began making a radio call. The VH aircraft lined up on the threshold. The Vixxen was unable to communicate location and needed to conduct a go-around. VH aircraft made another call. Sting made downwind call. Vixxen made upwind call. VH aircraft proceeded to take off while Vixxen was still on upwind and communicated that he was heading north and returning.
Shortly after, Vixxen made joining crosswind 21 call. VH aircraft stated that it was downwind 21. Vixxen could not locate aircraft. VH aircraft stated that it was downwind, over the Harbour on final. Sting asked for clarification of VH aircraft 's location. Vixxen located VH aircraft on straight in short final 21. VH aircraft landed, vacated the runway and taxied back to the hangar.
This occurrence has been referred to CASA for investigation. |