Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
21/4/2017 |
OCC1004 |
Albany |
WA |
Jabiru |
SP500 |
Jabiru |
Jabiru 2.2 |
The pilot Left the hangar at 9.25am, gave taxi call for RWY32, and then gave an entry and back track...
|
The pilot Left the hangar at 9.25am, gave taxi call for RWY32, and then gave an entry and back track call for 32. After which they gave a departure call on 32 stating they would be tracking 330. The pilot did not give an intended height as they intended to fly above the inversion which the pilot estimated to be about 4000ft. At approx. 7m N at about 3800ft. the pilot saw an incoming aircraft to Albany at a similar flight level slightly to their right. The aircraft was RPT. The aircraft also appeared to be taking evasive action to the left and passed to the right at a distance of about 300m. In the 15min that the pilots’ radio was on they was not aware of any incoming call. The pilot believes their radio was OK as there was other traffic at Albany and the RPT acknowledged that they had heard my departure call but that the pilot had not made a post take off call, which is correct, they intended to do so at 4000ft. The pilot is very aware of commercial aircraft at Albany and their priority, keeping to the E of any incoming or departing aircraft. RPT on radio said they had made a call. If this is so the pilot did not hear it.
Outcome: The reporting pilot carried out all required procedures at this non- controlled AD and was situationally aware of the general presence of RPT traffic. This incident highlights the overarching importance of well developed and practiced "See and Avoid" disciplines and appropriate avoidance action which were effectively applied in this instance. |
21/4/2017 |
OCC1011 |
10nm SE of Roma |
QLD |
Tecnam |
P92 Echo |
Rotax |
912 |
The engine began to intermittently run rough during cruise flight to a nearby airfield. Due to the n...
|
The engine began to intermittently run rough during cruise flight to a nearby airfield. Due to the northerly wind and altitude, it was decided to continue flying South to the intended airfield (4NM) but position the aircraft over open country in case it failed completely. An examination on the ground revealed one module to be very intermittent and the other to run rough at low engine revs. The maintainer installed two other modules to test engine and found it to run smoothly on one module and slightly rough on the other. The maintainer has now had three ignition modules that are in various states of failure.
OUTCOME: RAAus Technical Manager has reviewed this report and is aware of the known failure with this module in this type of engine. Technical Manager has spoken with the distributor in regard to this module and RAAus will continue to monitor these types of incidents. |
19/4/2017 |
OCC1006 |
Redcliffe Airport |
QLD |
Jabiru |
160C |
Jabiru |
2200B |
The aircraft experienced a total engine failure within the circuit area of Redcliffe Airport, the en...
|
The aircraft experienced a total engine failure within the circuit area of Redcliffe Airport, the engine stopped suddenly without prior indication. Normal engine failure procedures were undertaken and the aircraft was flown onto the approach of RWY07 at Redcliffe. Due to prevailing gusting winds at the time the aircraft contacted the ground in a sideways motion causing the nose gear to collapse with subsequent damage to the undercarriage and fuselage.
OUTCOME: Incident has been refereed to Airworthiness and Engineering branch of CASA. |
19/4/2017 |
OCC1003 |
Aldinga |
SA |
Cubcrafters Carbon Cub |
CC11-160 |
Cub Crafters |
CC340 |
Approximate wind at the time of the incident was 10kt NE. An unoccupied, un-chocked aircraft was par...
|
Approximate wind at the time of the incident was 10kt NE. An unoccupied, un-chocked aircraft was parked in a hangar with other aircraft. Personnel were taking the other aircraft out from the same hangar for the day and opened two doors on opposite sides of the hangar to make it easier to take out multiple aircraft. The doors remained open for approximately 5 minutes with no significant sign of wind blowing through the hangar. An unexpected strong gust of wind passed through the hangar, accelerating through the door opening causing the parked the aircraft to turn 90 degrees to the right. This caused the port wing to collide with the edge of the open hangar door which resulted in damage to the leading edge of the wing.
OUTCOME: When moving aircraft in and out of hangars, pilots must always be prepared for the possibility of thermal activity or unexpected gusts. Recommendations include closing the hangar doors once the aircraft is out, and chocking aircraft in hangars. Once out of the hangar, ensure the aircraft is parked with brakes secured or tied down for any extended periods prior to flying. |
18/4/2017 |
OCC1010 |
Gympie Airport |
QLD |
Auster |
J2 |
Textron Lycoming |
O-235-C1B |
Flying circuits at YGYM, Aircraft 1 was on short final RWY14, Aircraft 2: was on base. Aircraft 3 c...
|
Flying circuits at YGYM, Aircraft 1 was on short final RWY14, Aircraft 2: was on base. Aircraft 3 called entering and backtracking RWY14 just after Aircraft 1 called turning final. Aircraft 1 called short final to make Aircraft 3 known of their position. After Aircraft 3 realised the mistake, swerved erratically around runway but failed to vacate the RWY.
Aircraft 1 initiated a go around, Aircraft 2 shortly after was forced to go around for the same reason. On the next circuit, Aircraft 3 was still occupying the RWY, parked and not moving. The pilot of Aircraft 1 prompted and asked if they would vacate the RWY, Aircraft 3 replied that they were conducting run-ups on the RWY. Aircraft 1 initiated another go around as the RWY was blocked. Again Aircraft 1 prompted Aircraft 3 and asked if they would vacate the RWY, Aircraft 3 replied saying they were not on the pavement (but still on the grass within the gable markers, which is where Aircraft 1 intended to land). Aircraft 2 had to initiate another go around due blocked RWY.
A third go around initiated, Aircraft 2 landed on the pavement despite Aircraft 3 still being on the grass within the gable markers.
Aircraft 3 then vacated the RWY for a circuit. |
17/4/2017 |
OCC1020 |
Wollongong Regional Airport |
NSW |
Airborne Windsports |
XT 912 |
Rotax |
912 UL |
The aircraft bounced on landing, and on the second touchdown it veered to the left, coming to rest o...
|
The aircraft bounced on landing, and on the second touchdown it veered to the left, coming to rest on its right side in a water-filled ditch. The ditch was covered with long grass and it appeared as level ground.
OUTCOME: The student landed on an area outside the gable markers for the runway resulting in the aircraft diverting off track and subsequently impacting with a ditch. The aircraft was substantially damaged. The student will undertake additional training prior to issue of a Pilot Certificate. Members are reminded of the importance of landing within approved and appropriately maintained landing areas on aerodrome, as indicated by gable markers. |
15/4/2017 |
OCC1001 |
Moorabbin Airport |
VIC |
Aeroprakt |
Foxbat A22LS |
Rotax |
912 |
During circuit training on RWY 17L at YMMB, after making the final touchdown it was realised there w...
|
During circuit training on RWY 17L at YMMB, after making the final touchdown it was realised there was an aircraft on finals behind them so made the decision of exiting on RWY22. The pilot missed the turn on to taxiway Foxtrot and continued on RWY22. As soon as the pilot realised the error the pilot stopped and contacted YMMB ground. It was concluded that the aircraft had just crossed the holding point for RWY17R, which was also the duty RWY the time. The pilot had the gable markers ahead, indicating the entry into a RWY.
OUTCOME: A joint visit was undertaken between Airservices ATC staff, the school's training manager and RAAus Operations to identify specific operational issues and an appropriate working process to address these. Agreed attendance at monthly safety meetings by the Flight school and Airservices and the removal of a taxiway where regular occurrences have occurred has been applied as appropriate mitigation with continued monitoring being adopted. |
13/4/2017 |
OCC1005 |
Sunshine Coast Airport |
QLD |
Alpi |
Pioneer 300 |
Rotax |
912 ULS |
During a training circuit it was noted the engine was running rough on approach. At first it was sus...
|
During a training circuit it was noted the engine was running rough on approach. At first it was suspected icing and the pilot took appropriate actions with no improvement. By the time the aircraft was on short final, below 200ft approximately the rough running drastically escalated resulting in the engine failing completely. The aircraft landed safely and some basic checks carried out on the RWY resulting in restarting the engine.
OUTCOME: Upon Inspection of the aircraft (by the engineer responsible for the usual maintenance) it was confirmed to have been a failure in the mechanical fuel pump. Although the electrical auxiliary pump was running at the time this particular failure still resulted in loss of power. This is a type certified engine in the pioneer. |
12/4/2017 |
OCC1000 |
Tunbridge Airfield |
TAS |
Jabiru |
J120C |
Jabiru |
2200 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft landed with a flat main wheel tyre, damaging the...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft landed with a flat main wheel tyre, damaging the disc rotor. Due to the design of the brakes, the brake disc diameter is larger than the rolling flat tyre diameter of the wheel. This can allow the disc rotor to freely roll on the runway surface causing bending and burring damage to the thin disc, rendering it u/s or worst case, jamming in the caliper assembly, locking the wheel from turning.
DETERMINED OUTCOME: This occurrence has been referred to CASA engineering and airworthiness branch and the manufacturer for further monitoring and action where required. |
11/4/2017 |
OCC0994 |
~20Nm E of Cunnamulla |
QLD |
Kitfox |
Speedster |
Rotax |
912 |
After an uneventful take off the pilot proceeded to make track and climb on a heading of 000 towards...
|
After an uneventful take off the pilot proceeded to make track and climb on a heading of 000 towards Charleville. At an altitude of about 2700ft the pilot started to smell a faint smell of oil and was proceeding to re-scan the gauges, when sparks erupted from under the cowl and the engine lost power. The pilot cycled the magnetos and established there was no power. The pilot then switch off magnetos, made two May-Day calls on the area frequency and the multi-com frequency and commenced a gentle turn away from a wooded area towards more open country to the south nearer to a Farmstead. The pilot selected a landing site that was clear of large trees and that had less shrub and proceeded to land, but as the aircraft was slowing the right wing collided with a small dead tree. The aircraft then ground looped in a clockwise direction and came to stop. The pilot then self extracted without harm and proceeded on foot the homestead to raise the alarm.
DETERMINED OUTCOME: The aircraft is a 19 amateur built but had a type certified 912 A rotax. Aircraft has a total time of approx 470 hours in 24 years. The problem was identified as a value issue but until the engine is pulled down nothing further at this stage. The aircraft and engine was L2-LAME maintained. The owner stated that the engine appeared to run a little rough prior to take off. In time a pull down report may be supplied. |
8/4/2017 |
OCC0988 |
Geraldton |
WA |
Morgan Aero Works |
Cougar MK1 |
Jabiru |
3.3 |
Whilst the aircraft was taxiing the nose wheel became stuck in loose dirt. Over use of right rudder ...
|
Whilst the aircraft was taxiing the nose wheel became stuck in loose dirt. Over use of right rudder by the pilot caused rudder cable to break.
OUTCOME: This is an amateur built aircraft where the design standards are not mandated. On review of similar types of aircraft it has been identified that a bike brake cable is sometimes used in this application and is usually supplied with the kit. The RAAus Technical Manager has spoken with the aircraft designer of this amateur build regarding parts. |
8/4/2017 |
OCC0995 |
Loxton Airfield |
SA |
Challenger |
CH2 |
Rotax |
503 |
The aircraft was tied down alongside the hangar when a very strong gust of wind broke the tie down r...
|
The aircraft was tied down alongside the hangar when a very strong gust of wind broke the tie down ropes and flipped the plane upside down, resulting in the wing landing on a club members’ car.
OUTCOME: A freak convection gust (which was later reported to exceed 70kph caused the aircraft to lift from its tie downs which were tied down to water ballast containers). Consequently one rope failed when the aircraft was lifted and one rope attached to a water container snapped allowing the aircraft to flip over an adjacent fence and onto the car. No weather conditions were forecast to indicate extreme convection, storm or frontal activity according to owner. |
1/4/2017 |
OCC1013 |
Gawler Airfield |
SA |
Zenith Aircraft |
Zodiac Ch 601 Hds |
Rotax |
912 UL |
As the pilot was turning right onto downwind, a glider was coming towards the aircraft from the slig...
|
As the pilot was turning right onto downwind, a glider was coming towards the aircraft from the slight right hand side (up the downwind). The pilot took action to avoid the glider as did they, the pilot radioed the glider to say they had been seen and avoided, however got no response.
OUTCOME: The incident has been reported to the Gliding Club safety committee and CFI for follow up. It is likely it was a glider and pilot not familiar with the airfield and right hand circuits on RWY 23, the actions from the gliding club address any identified issues. RAAus Operations Manager has reviewed the report, no further action at this time. |
1/4/2017 |
OCC0989 |
Wedderburn |
NSW |
Storm |
Rally |
Rotax |
912 ULS |
On flight from Wollongong to Wedderburn oil pressure dropped to 0.8 Bar which is well below the mini...
|
On flight from Wollongong to Wedderburn oil pressure dropped to 0.8 Bar which is well below the minimum of 2 Bar for the Rotax 912 ULS type. The pilot made a call to alert other traffic to the inflight emergency and priority given. An uneventful landing was made.
An examination showed the lid on the oil tank had tilted up on one side allowing oil to escape. Residual oil in tank was found to be 600mm. Oil was replaced, the system purged of air and the oil pressure on start-up returned to normal. Compression afterwards was as expected and no damage to engine evident. During the emergency the CHT remained stable at 100 degrees C which is normal and the oil temperate was not elevated.
DETERMINED OUTCOME: It is likely that this issue occurred due to a faulty O-ring on the oil tank. Owner operator reminded to review LSA manufactures maintenance schedule. |
29/3/2017 |
OCC0991 |
Dalby |
QLD |
Sonex |
Sonex |
Jabiru |
33A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The green urethane hose used on static, pitot and fuel lines ...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The green urethane hose used on static, pitot and fuel lines have aged quickly and become very brittle and will crumble at the slightest touch or vibration.
Determined Outcome: RAAus Technical department has suggested that the hoses be replaced and that the L2 discusses ongoing airworthiness with the owner of the this aircraft. As a 19 amateur built members are free to trial times that may not be deemed suitable in normal engineering activities. |