Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
25/2/2017 |
OCC0939 |
French Island |
VIC |
Aeroprakt |
A22LS Kelpie |
Rotax |
912 ULS |
The pilot landed the aircraft on a beach, then taxied to what appeared to be a flat rocky surface, h...
|
The pilot landed the aircraft on a beach, then taxied to what appeared to be a flat rocky surface, however this turned out to be mud with about 20cm of water beneath the surface. The nose wheel then sank under the mud and the aircraft bogged. The pilot turned the engine off and tried to pull the aircraft from the soft ground and to locate firmer ground to take off from. When the pilot started the aircraft and tried to taxi the aircraft to the harder ground it bogged again, this time with the tip of the propeller making contact with the muddy ground. The pilot immediately shut the engine down, closed the fuel valves for both wings and turned off the electric system of the aircraft then called for assistance as it was unknown how long it was until high tide.
OUTCOME: The pilot elected to land on a beach however the surface was not appropriate and the aircraft became bogged. The pilot moved the aircraft to what was believed to be a more suitable location, however during the take off roll the aircraft sank into soft sand and the propeller impacted the sand. The aircraft was disassembled and removed for an assessment of the engine to ensure no damage occurred. The pilot has undertaken further research and determined landings on beaches must include an independent assessment of the surface suitability prior to landing. |
25/2/2017 |
OCC0943 |
Private strip, Bluewater |
QLD |
Aeroprakt |
A22LS Foxbat |
Rotax |
912ULS |
Upon return to a private strip, after waiting for a local shower to pass, the pilot carried out a no...
|
Upon return to a private strip, after waiting for a local shower to pass, the pilot carried out a normal approach and landed. The strip had just been mown and was covered with grass which caused the aircraft to skid when the brakes were applied. The aircraft overran the strip impacting with the fence at the end of the RWY. Upon exiting the aircraft it was noted that the prop had impacted a star picket and there was some minor damage done to the cowlings and a branch had touched the leading edge of the left wing leaving a small indent and scratching underside of left flaperon.
OUTCOME: RAAus Operations Managers have reviewed this report and the pilot identified that due to the wet grass (that was cut that day) it caused an increase of the aircraft speed off the runway. The pilot also observed that the wind had dropped to nil which also was a factor. Additionally the limited overshoot area contributed to the incident and with an additional 20 metres or more would have avoided any impact. As such the private strip will now be extended to overshoot / undershoot by 75 metres and include an installation of a 2.8 metre windsock. |
23/2/2017 |
OCC0934 |
Goulburn |
NSW |
Skyfox |
Gazelle |
Rotax |
912A |
A student was conducting solo circuits with conditions that were CAVOK with light winds. The aircraf...
|
A student was conducting solo circuits with conditions that were CAVOK with light winds. The aircraft experienced rough running, with engine noise and partial power loss on upwind RWY 04. The student performed a successful forced landing straight ahead into a paddock approximately 1.5 NM NW of the field.
OUTCOME: On inspection of the engine the maintainer found the Carby circlip was unserviceable. The aircraft has now been fitted with a new circlip and the aircraft is again serviceable. |
22/2/2017 |
OCC0947 |
Moree |
NSW |
Tecnam |
P92 Echo |
Rotax |
912S |
The pilot was unaware that their taxi broadcast was not heard, nor did they hear any readable incomi...
|
The pilot was unaware that their taxi broadcast was not heard, nor did they hear any readable incoming aircraft calls. The pilot first saw another aircraft on the TWY, where the two aircraft passed each other safely. When stopped at the holding point the pilot heard a third aircraft for the first time, when it broadcast overhead and joining the circuit. The pilot broadcast that they were backtracking to the RWY, took off, and made a departure call. It's possible that the radio malfunctioned, or was not receiving on 126.7 - equally possible for other aircraft to have unexplained transmission issues. OAT was extreme - at least 45C. The pilot had communicated with aircraft other than these two on 126.7 both before landing and after departing the airfield on this day.
OUTCOME: The Pilot in command did not use effective see and avoid strategies relying on radio for primary separation. Further contributing factors were incorrect taxiing procedures and application of correct give way rules. RAAus Operations have provided education and training to the pilot on further risk mitigation and lookout techniques. |
21/2/2017 |
OCC0941 |
Bendigo |
VIC |
Tecnam P92 |
P92 Echo Super |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: As per normal practice, the pilot checked each igniti...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: As per normal practice, the pilot checked each ignition circuit before shutting down the engine by turning off each mag switch in turn. When the right hand switch was turned off there was a dead cut of the engine. The engine was restarted and tested at normal run up revs of 3800 and then at 3000 and found it was OK, however when it was checked at 2000 rpm an intermittent fault was found. Switches, wiring and plug connectors were tested and found OK. The ignition modules were tested by substitution of a spare module and the problem was found to be rectified.
OUTCOME: The National Technical Manager has reviewed all data and is satisfied all areas of concern have been addressed. Unfortunately the ignition modules do fail and this has been addressed by RAAus with the Australian importer. |
21/2/2017 |
OCC0929 |
Tooradin Airfield |
VIC |
Airborne |
Edge XT 912 |
Rotax |
912 UL |
The pilot was standing beside the cockpit, with left foot on the brake, left hand on the compression...
|
The pilot was standing beside the cockpit, with left foot on the brake, left hand on the compression strut while pressing the start button with the intention that once the engine started, removing a heat pack from the ignition module, then climbing into the cockpit.
On starting, the plane rolled forward. Pressure on the left brake pedal served only to turn the nosewheel to the right and the brakes to be not applied. The pilot swung into the cockpit but could not regain sufficient control before the plane rolled 15m and the left wing struck a light pole. The power of the engine caused the nose to rise up the light pole, the left landing gear strut contacted the light pole, and the plane came to rest in a nose up position resting on the engine and propeller.
OUTCOME: Loss of Control of aircraft during starting phase due to pilot not being correctly seated and in control of the aircraft braking systems |
20/2/2017 |
OCC0932 |
Yarrawonga |
VIC |
Airborne |
XT 912 |
Rotax |
VL180 |
The aircraft crossed the threshold slightly high but still within the limits of a normal approach an...
|
The aircraft crossed the threshold slightly high but still within the limits of a normal approach and landing. It is unclear if the student then took the power off and put an incorrect input in. The aircraft lurched to the left and descended rapidly to the ground, hitting the left wheel first. The instructor grabbed the controls and told the student to add full power. The aircraft bounced on the left wheel and we were airborne again. The instructor subsequently requested the student select full power as he could not get to the throttle as he had both hands on the controls. The aircraft became airborne again but not lined up on the runway. Again the instructor requested full power however there was no input from the student. On the third bounce the aircraft settled on the runway but it was angled to the left and slowing down. This is when the student added full power. The aircraft then rapidly started moving towards the fence past the flight strip. The instructor had the controls but not the throttle. The aircraft became airborne again and began to climb. The instructor’s intention was to conduct a go-round until the student then put the throttle to flight idle. This caused the aircraft to descend hitting the top of the fence and the aircraft rolled slowly over the fence inverted and settled on its right side.
OUTCOME: A full investigation including a school inspection and CFI renewal was conducted to review training processes and instructional flight management relating to recovery from uncontrolled states both in generic weight shift environments and further into control protocols and risk management in weight shift instructional environments. The investigation outcomes have resulted in adaption by the CFI and school of a more robust application of risk principles in flight operations.
It is further recommended by operations that where shared control environments are required that early intervention of potential uncontrolled states be adopted by all instructors and briefed accordingly in regards to HF elements of pre-flight and operational briefings in relation to crew responsibilities and cockpit resource management (CRM). |
18/2/2017 |
OCC0925 |
Brisbane West Wellcamp |
QLD |
Jabiru |
J160C |
Jabiru |
2200 B |
Conducting touch and go's, the aircraft came to a full stop landing. The pilot then applied full pow...
|
Conducting touch and go's, the aircraft came to a full stop landing. The pilot then applied full power to take off and after 25-40 meters into wind, the Port wing rose suddenly and the aircraft "wheel barrowed" on the front wheel and starboard main wheel, striking propellor and just touching starboard wingtip. The aircraft then righted itself, and came to a stop.OUTCOME: Runway Loss of Control event R-LOC. PIC has undertaken additional training and counseling. |
18/2/2017 |
OCC1069 |
Morton Island |
QLD |
Flysynthesis |
Texan 550 |
Rotax |
912 ULS |
The PAX unlatched one side of the bubble canopy of the aircraft while in flight. A precautionary lan...
|
The PAX unlatched one side of the bubble canopy of the aircraft while in flight. A precautionary landing was safely carried out at local airfield.
OUTCOME: Operations Managers have reviewed this report and no further action or comment is required. Members are reminded to ensure that all passengers have had a pre flight briefed conducted. |
16/2/2017 |
OCC0922 |
Noosa Heads |
QLD |
Alpi |
Pioneer 200 |
Rotax |
912 ULS |
A delayed inbound call owing to unusually high volume of radio traffic resulted in the aircraft to b...
|
A delayed inbound call owing to unusually high volume of radio traffic resulted in the aircraft to be within the airspace prior to being able to contact ATC. The pilot then misunderstood the tower instructions for approach to maintain 1500' and join L downwind 36 and was on track to join R downwind 36 before further contact with the tower for correction.
OUTCOME: RAAus Operations Managers reviewed this incidents with the Aero Club CFI and noted that the member was exercising the privileges of his CASA RPL not any RAAus exemption privileges. Notwithstanding this the pilot has been debriefed on CTA clearance protocols. |
12/2/2017 |
OCC0915 |
Ball Bay |
QLD |
BRM Aero |
Bristell UL FG |
Rotax |
912 ULS2 |
The aircraft had been flying for approx. 30 minutes at 5,000 RPM and 2,000ft when there was a slight...
|
The aircraft had been flying for approx. 30 minutes at 5,000 RPM and 2,000ft when there was a slight shudder and the revs dropped to 3,800 RPM. The fuel pressure was 4 PSI and all instruments checked okay. The pilot pulled on the carby heat and turned the electric pump on - fuel pressure was at 5 PSI. Revs dropped slightly and as the pilot was close to Ball Bay airstrip carried out a precautionary landing with no incident. On the ground and engine would not rev above 3,800 RPM.
Determined Outcome: This incident has not been able to be replicated on the ground. The carburettor and ignition were replaced with no reoccurrence. The conditions on the day of the incident were; temperature 32 degrees with 60% humidity and may have been a contributing factor. The RAAus Technical Manager has made the LSA importer aware of this issue so that they can monitor any future occurrences. No further action by RAAUs can be taken at this point in time. |
12/2/2017 |
OCC0914 |
Atherton Airport |
QLD |
JABIRU |
J230 |
Jabiru |
3300 |
After completing pre-flight checks the pilot taxied to the runway threshold and lined up for take-of...
|
After completing pre-flight checks the pilot taxied to the runway threshold and lined up for take-off. After giving a rolling call, full power was applied and initial speed pick up was good but as the aircraft went up the hill it didn't pick up in the long wet grass. On the flat it slowly picked up speed in the long wet grass however the pilot felt there was not enough runway left so, closed the throttle and applied the brakes. The brakes locked and skidded so the pilot released them and reapplied several times, not as hard, then started to make a right turn but was still too fast. The pilot was concerned that the left wing would contact the ground so decreased the turn. Then the aircraft slid into a fence hitting a post which caused a prop strike, then bounced back and the tail made contact with a post at the back.
OUTCOME: Pilots are reminded to consider appropriate Take off rejection points as part of their Pre Take-off safety brief with particular consideration to variations in slope of runway and surface conditions. |
12/2/2017 |
OCC0920 |
Walgett |
NSW |
Cessna |
162 |
Continental |
0-200-D |
Birdstrike: The pilot observed a number of birds around the runway however they flew away while the ...
|
Birdstrike: The pilot observed a number of birds around the runway however they flew away while the aircraft was taxied and touch and goes were conducted. When conducing the final landing, a few birds did not fly away and hit the aircraft wing.
OUTCOME: RAAus have checked the ERSA for Walgett to confirm information is available about bird hazards. The ADDITIONAL INFORMATION section states:
1. After rain deep water puddles. ACFT 5,700KG & ABV confine TAX to RWY centre & turn
only on RWY end turning nodes, 05/23.
2. Animal & bird hazard exists.
RAAus will continue to monitor for any additional reporting of additional bird strikes. |
11/2/2017 |
OCC0916 |
Quirindi Airport |
NSW |
Aeroprakt |
A22LS Foxbat |
Rotax |
912 U L S |
The aircraft suffered a heavy landing causing nose wheel leg to be bent.
Determined Outcome: Due ...
|
The aircraft suffered a heavy landing causing nose wheel leg to be bent.
Determined Outcome: Due to the approach speed not being managed appropriately, the aircraft suffered a hard landing and damaged the nose gear. PIC noted HF and inappropriate approach speed and steep angle. Pilots are reminded of the importance of a stabilised approach at the manufacturer's recommended speed according to the POH. |
10/2/2017 |
OCC0985 |
Maroochydoore |
QLD |
AeroPrakt |
A32 |
Rotax |
912 ULS |
The light aircraft did not receive calls from ATC therefore failed to respond. This resulted in an R...
|
The light aircraft did not receive calls from ATC therefore failed to respond. This resulted in an RPT having to cancel an already cleared RNAV-36 (RNP) approach. The RPT subsequently joined a Visual Right CCT. Communications were re-established between ATC and the light aircraft.
OUTCOME: Temporary loss of 2 -way communications between tower and aircraft. No cause was able to be identified. |