Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
5/1/2017 |
OCC0885 |
Moorabbin Airport |
VIC |
Aeroprakt |
A22LS Foxbat |
Rotax |
912 |
Runway Incursion: After making a full stop landing at YMMB on RWY35R and taxiing onto taxiway Bravo,...
|
Runway Incursion: After making a full stop landing at YMMB on RWY35R and taxiing onto taxiway Bravo, the pilot made a call to taxi to the main apron. As soon as the pilot finished the call they heard another call which was "taxi to the main apron." The pilot assumed this was tower but in fact was another aircraft. The pilot gave a read back call which may not have transmitted due to the microphone button not being pressed all the way. After not hearing anything after read back, the pilot assumed that the aircraft was cleared to cross the active runway.
OUTCOME: The pilot misunderstood calls as originating from the tower and taxied without clearance. In future, the pilot will ensure the call originated from the tower and that calls are directed at them by listening for their call-sign. |
30/12/2016 |
OCC0867 |
Moorook |
SA |
Jabiru |
SK4 |
Jabiru |
2200J |
Initial report stated that the aircraft experienced a rough running engine when coming into land in ...
|
Initial report stated that the aircraft experienced a rough running engine when coming into land in a field, where the aircraft struck power lines. Aircraft has been destroyed and the pilot and passenger had minor injuries.
OUTCOME: RAAus Operations had discussions with PIC regarding possible casual factors which led to this incident. PIC admit that the aircraft did not experience engine difficulties and that they were actually flying low causing the aircraft to strike power lines. Operations has proposed for the PIC to complete a Low Level (LL) training (not for issues of LL endorsement, for educational purposes) with an appropriately endorsed CFI prior to any further flight. |
29/12/2016 |
OCC0865 |
Saint Helens |
TAS |
Icp Srl |
Savannah VG |
Rotax |
912ULS |
In the final stage of flight (near final destination) the pilot noticed fog was obscuring the airstr...
|
In the final stage of flight (near final destination) the pilot noticed fog was obscuring the airstrip and made the decision to land on the sand at a nearby beach. After very gently touching down, the front wheel became stuck in 4x4 ruts and collapsed which caused aircraft to flip onto its back. No injuries were sustained by the pilot.
OUTCOME: Weather deteriorated faster than forecast and fog accumulated at the airport, with less than 2 NM to run. As there were no other nearby airstrips within safe decision making distance, the pilot elected to conduct a precautionary landing on the beach rather than arrive at an alternate with minimal fuel remaining. He elected not to attempt to land at the airstrip through the fog even though his GPS told him it was only 2 NM away. The pilot had sufficient fuel to conduct orbits and assess the situation, prior to conducting a precautionary landing on the beach. The aircraft flipped onto its back due to soft sand with no injuries to the pilot. A review of weather and assessment of beach landing considerations will be conducted at the next flight review. |
29/12/2016 |
OCC0866 |
Tumut |
NSW |
Zenith Aircraft |
Zodiac 601 Xl |
Jabiru |
3300A |
While starting the engine the pilot accidentally had a small amount of throttle on which caused the ...
|
While starting the engine the pilot accidentally had a small amount of throttle on which caused the aircraft to surge forward and hit the adjoining hangar. Some damage was sustained to the aircraft propeller and wingtip, with the hanger receiving a dent in one corner.
OUTCOME: While starting the aircraft, the appropriate actions to prevent the aircraft moving were not enacted which resulted in the aircraft striking a hangar with the wing tip and propeller. Members are reminded of the importance of checklists and appropriate actions when starting or shutting down an aircraft to prevent injury to bystanders, other aircraft or buildings. |
28/12/2016 |
OCC0871 |
Aldinga Airfield |
SA |
Evektor |
Sportstar SL |
Rotax |
912ULS |
Aircraft commenced take off roll and just got airborne when engine lost some power. Take off aborte...
|
Aircraft commenced take off roll and just got airborne when engine lost some power. Take off aborted and aircraft landed safely on remaining runway and taxied back to hangar.
OUTCOME: On inspection of the aircraft to determine the cause of engine power loss the maintainer found that it was due to a valve in the engine fuel pump. Owner has contacted the distributed who will be conducting further analysis on the pump. Fuel pump has been replaced and the aircraft is again serviceable. |
28/12/2016 |
OCC0870 |
Aldinga Airfield |
SA |
Evektor |
Sportstar |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Failure of the outlet valve in the fuel pump caused a...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Failure of the outlet valve in the fuel pump caused a loss of power on take-off. Take-off aborted and aircraft landed on remaining runway. Part of the valve is pressed into the body of the pump. The part pressed into the body came out after - the outlet valve remained open which caused a drop in the fuel pressure. Note: the standby electric pump was 'On' however also lost pressure through this failed valve.
OUTCOME: This aircraft is an LSA and as such this defect was reported to the manufacturer. Technical Manager reviewed the aircraft logbooks which was provided by the maintainer. The aircraft logbook showed that it has high hours and appears the fuel pump has failed due to fair wear and tear. |
23/12/2016 |
OCC0864 |
Caboolture |
QLD |
Foxbat |
A22LS |
Rotax |
912 ULS |
While on base leg (instructor conducting circuits with a student) the pilot suggested bringing on po...
|
While on base leg (instructor conducting circuits with a student) the pilot suggested bringing on power to check the aircraft's rate of descent as they were about to turn final and did not want to drop below 500 ft (the aircraft altitude was approximately 600 ft). As the power was increased, the engine shook violently and stopped almost immediately. Upon finding a safe place to set it down, the pilot turned on both fuel taps and managed to restart the engine. The pilot returned to the airfield with no further incidents.
OUTCOME: Technical Manager reviewed of the report and noted that the possible cause may have been either the fuel taps being turned off or also a possible issue with the fuel return line. This aircraft has recently had issues highlighted regarding the fuel return line which has been addressed by manufacturer. The manufacturer has proved service kits to owners in order to address any issues regarding fuel return line. |
23/12/2016 |
OCC0940 |
The Oaks |
NSW |
Jabiru |
J230 D |
Jabiru |
|
The engine started to run rough approximately 12NM from the airfield. The pilot returned to the airf...
|
The engine started to run rough approximately 12NM from the airfield. The pilot returned to the airfield, when on late finals the engine cut out. The aircraft landed successfully with no damage or injury.
OUTCOME: RAAus Technical Manager spoke with the pilot/ owner who stated that the engine issues appeared to be due to the exhaust value breaking which caused a catastrophic internal failure of the engine. The pilot/ owner has been working closely with the manufacturer who have provided a brand new engine with roller rockers and a redesigned cam profile which will remove some of the cam pressure on the value train. |
23/12/2016 |
OCC0874 |
Lethbridge Airport |
VIC |
Jabiru |
SP500 |
Jabiru |
2200 |
The aircraft was taxied along the grass taxiway running parallel to RWY10, upon reaching a position ...
|
The aircraft was taxied along the grass taxiway running parallel to RWY10, upon reaching a position adjacent to the "Piano Keys" the aircraft was turned at 90 degrees to the runway direction to enter the runway just short of the threshold gable markers. Unseen by the pilot was an unmarked drain/culvert which also ran parallel to the runway and was hidden from sight by the grass. As the aircraft began to cross the drain, the propeller tips encountered the earth on the far side if the depression delaminating them for a length of approximately 70mm. The aircraft was withdrawn from service until a replacement propeller was fitted and the Jabiru post prop strike procedure was completed.
OUTCOME: While taxiing, the pilot was not aware of a depression in the ground in the grass, resulting in a propeller strike. All required actions after propeller strike now conducted. |
22/12/2016 |
OCC0862 |
Moorabbin Airport |
VIC |
Aeroprakt |
AP22LS Foxbat |
Rotax |
912 ULS |
The pilot misunderstood instructions from ATC resulting in incorrectly joining the circuit. The pilo...
|
The pilot misunderstood instructions from ATC resulting in incorrectly joining the circuit. The pilot received further instructions from the controllers and then clearance to land.
OUTCOME: RAAus Operations reviewed the report and found that the error in CTA procedures was due to expectation bias. The day prior to the pilot had been operating on a different runway due to the normal runway being unavailable, which meant that they were conducting unusual operations for the aerodrome. The pilot believed that the confusion was due to the combination of the operations that were being conducted the previous day and a misunderstanding of the controllers instructions as factors that contributed to this incident. NFA required. |
17/12/2016 |
OCC0888 |
Port Macquarie |
NSW |
Aeroprakt |
A22LS FOXBAT |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: There have been cracks found in the radius of the ben...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: There have been cracks found in the radius of the bend on both sides of the doubler bracket at rear wing attach point on the through spar. There are also cracks coming from some of the rivet holes.
OUTCOME: As this aircraft is a LSA this defect was referred to the manufacturer. The factory has supplied new brackets for replacement in the aircraft and are reviewing images of the brackets in question. The factory are reviewing the part to identify weather it is considered to be a design issue or operational (due to a heavy landing however will issue a revision or update if required. |
16/12/2016 |
OCC0921 |
Sunshine Coast Airport |
QLD |
The Aeroplane Factory |
Sling 2 |
Rotax |
912 ULS |
After landing on RWY 36, instead of rolling through to the next taxiway (Alpha), the pilot requested...
|
After landing on RWY 36, instead of rolling through to the next taxiway (Alpha), the pilot requested backtrack on RWY 18 and commenced a backtrack turn without waiting for clearance. ATC then advised that clearance was required prior to backtracking, and then provided a clearance to the pilot.
OUTCOME: Pilot was in the middle of requesting clearance from Surface Movement Control (SMC) when he initiated back track. Pilot has discussed the occurrence with the CFI and remedial action has been taken to address CTR and clearance requirements. |
16/12/2016 |
OCC0863 |
Sunshine Coast |
QLD |
The Airplane Factory |
Sling 2 |
Rotax |
912 ULS |
A student pilot was on a solo flight in circuit area and was in the flare when the aircraft was stru...
|
A student pilot was on a solo flight in circuit area and was in the flare when the aircraft was struck with a gust of crosswind. The student managed to keep the aircraft pointed in the right direction, but allowed the wind to drift the aircraft off the runway, resulting in the student landing on the grass next to the runway. The student then took off again, completing a circuit with a full stop landing.
OUTCOME: RAAus Operations have reviewed this report. Minor runway loss of control which was recovered by the pilot. |
15/12/2016 |
OCC0854 |
Moorabbin Airport |
VIC |
Bristell |
FG |
Rotax |
912 ULS |
Briefing a student on HARRT check (Height, ATIS, Runway, Radio, Transponder) inbound to (prior to ar...
|
Briefing a student on HARRT check (Height, ATIS, Runway, Radio, Transponder) inbound to (prior to arriving at) Carrum (CARR). Both instructor and student briefed that it was RWY 13R in use. Upon arriving at CARR radio congestion from outbound traffic led to student delivering inbound radio call just past CARR. While listening and looking out for any inbound and outbound traffic on radio, the instructor told the student to track towards Mordialloc pier and descend to circuit height of 1000ft. This tracking led the instructor to believe that the aircraft would then join the circuit for 17R and as such then instructed the student to turn right and join onto downwind (and make a joining downwind radio call at this position). They proceeded to follow this circuit pattern. While on downwind the instructor began briefing student on before landing checks as they previously could not complete them due to looking and listening out for traffic. Turned onto base RWY 17R and heard tower tell traffic behind to “follow Bristell turning onto final”. The instructor was confused by the tower instructions as they had only just turned onto base and thought that they had overestimated their speed and position in the circuit pattern. At this point the instructor identified the Foxbat traffic on an opposing circuit and was about to confirm if it had now joined their circuit ahead of them to land. Before this could be done the tower contacted the instructor and student saying that they had gone past final for RWY 13R and had maybe aligned for RWY 17R. The tower instructed to make the corrections and a safety alert was issued. Immediately the instructor took over and made corrections back to final for RWY 13R. There were no further problems and the instructor called tower after landing.
OUTCOME: CFI debriefed instructor and matter was raised and resolved at Moorabbin Safety meeting. No further action required. |
15/12/2016 |
OCC0850 |
Bundaberg Airport |
QLD |
Jabiru |
J120 |
Jabiru |
2200 |
The aircraft landing was uneventful, however the right hand tyre deflated during the rollout. The ai...
|
The aircraft landing was uneventful, however the right hand tyre deflated during the rollout. The aircraft was pushed clear of the main RWY. The tyre and tube were replaced and the aircraft taxied back to the hanger.
OUTCOME: On inspection of the tyre a 8 mm long piece of wire was found and removed (which caused the tyre to deflate). The tyre and tube have been replaced and aircraft operatable. |