Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
12/12/2017 |
OCC1232 |
Archerfield Airport |
QLD |
The Aircraft Factory |
Sling LSA |
Rotax |
912IS |
During the run up checks the coolant temperature went briefly above the operational limits dropping ...
|
During the run up checks the coolant temperature went briefly above the operational limits dropping within normal range during the take-off run.
Outcome: No action required by RAAus. |
12/12/2017 |
OCC1229 |
Private Airstrip, Mt Garnet |
QLD |
Skyfox Aviation |
Gazelle |
Rotax |
9120 A2 |
A loud bang /backfire was heard from the engine after take-off at approx. 250ft. and the prop ceased...
|
A loud bang /backfire was heard from the engine after take-off at approx. 250ft. and the prop ceased turning instantly. The pilot conducted a forced landing into a paddock where the front wheel hit rocks in long grass and collapsed. The aircraft came to rest in a steep nose down attitude. Fuel was poured from both tanks resulting in the aircraft catching fire moments later.
DETERMINED OUTCOME: RAAus is unable to determine the cause of this occurrence. It is possible that the occurrence was attributed to extended periods of sitting and no use. |
10/12/2017 |
OCC1228 |
Narrabri |
NSW |
Tecnam |
Sierra |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Inspection of the engine during routine maintenance r...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Inspection of the engine during routine maintenance revealed that the upper through bolt to Cylinder #1 had sheared off and the head bolt nut on cylinder #1 had come off.
Outcome; Referred to CASA Airworthiness and Engineering Branch. |
8/12/2017 |
OCC1235 |
Sunshine Coast Airport |
QLD |
The Aeroplane Factory |
Sling 2 |
Rotax |
912 ULS |
The RAAus aircraft reported ready at holding point C for RWY36. A GA aircraft was on final with a l...
|
The RAAus aircraft reported ready at holding point C for RWY36. A GA aircraft was on final with a landing clearance and the RAAus was given a conditional line up clearance behind. The RAAus aircraft was observed to taxi forward and enter the flight strip RWY36.
DETERMINED OUTCOME: The CFI has taken appropriate action to remediate those involved. No further action by RAAus required. |
7/12/2017 |
OCC1231 |
Orange |
NSW |
Jabiru |
J160 |
Jabiru 2200 |
J2200B |
The pilot landed aircraft while transmitting on the incorrect frequency. They appear to have bumped ...
|
The pilot landed aircraft while transmitting on the incorrect frequency. They appear to have bumped the mode switch while in the circuit causing the radio to be on the incorrect frequency.
DETERMINED OUTCOME: Operator error, no further action required. |
5/12/2017 |
OCC1227 |
Moorabbin Airport |
VIC |
Aeroprakt |
Foxbat A22LS |
Rotax |
912 ULS |
The aircraft departed to the south for an instructional flight in the YMMB training area from RWY 31...
|
The aircraft departed to the south for an instructional flight in the YMMB training area from RWY 31R. Standard procedure for a departure to the south is a right hand circuit however, the pilot made a left had turn. Usually RWY 31R is for Circuits at YMMB, and the instructor mainly use 31L for departures to the south. However, on this date, only RWY 31R was in use as per NOTAM and Circuits were not being done. The instructor didn’t recall departures from 31R were in the opposite direction and conducted a departure as if they were taking off on 31L. Tower notified the pilot of the error but as there was no risk of collision with another aircraft they continued with the original departure track.
DETERMINED OUTCOME: This procedural error was reviewed with CFI and instructor involved who was very experienced but new to Moorabbin operations. Understanding of local procedures has been corrected and reassessed for this aerodrome. |
5/12/2017 |
OCC1224 |
Cunnamulla Airport |
QLD |
Tecnam |
P 2004 Bravo |
Rotax |
912 ULS |
During flight training, a student on one of their last flights prior to the Pilot Certificate practi...
|
During flight training, a student on one of their last flights prior to the Pilot Certificate practical examination was conducting a 4 mile final straight in approach on RWY 30. In the flare, hold off the student got it crossed up and landed slightly heavy not aligned with the runway. There was a noise and a thud and the instructor thought that a wheel bearing had collapsed or a flat tyre and immediately tried to regain control of the aircraft keeping what they thought was a damaged wheel off the ground and holding the nose up to protect the propeller/engine.
The touch down happened on the 500ft marker and the instructor kept directional control till the 1500ft marker where the plane ground looped just outside the gable markers. The wheel and landing gear leg was 20m from where the aircraft stopped. The saddle that holds the landing gear leg was located on the 500ft marker where the wheel impacted the ground.
DETERMINED OUTCOME: The school has identified that it is possible that an unreported incident may have contributed to this occurrence. It is not possible to determine the cause however the school as taken all reasonable action to address the issue by enforcing a 500 hourly bolt replacement and increased safety communication WRT reporting of incidents |
3/12/2017 |
OCC1220 |
Private Airstrip, Emerald |
QLD |
Jabiru |
J230 |
Jabiru |
3300 |
The aircraft ran off the airstrip and the nose wheel collapsed in mud.
OUTCOME: The aircraft has ...
|
The aircraft ran off the airstrip and the nose wheel collapsed in mud.
OUTCOME: The aircraft has been referred to the RAAus Tech team to ensure the aircraft undergoes appropriate repairs before returning to the air. |
29/11/2017 |
OCC1223 |
Warnervale Airport |
NSW |
Foxbat |
A22LS Amphibian |
Rotax |
912 ULS |
Pressure was lost in undercarriage operating system. The undercarriage was lowered and visually conf...
|
Pressure was lost in undercarriage operating system. The undercarriage was lowered and visually confirmed it was down but locked down could not be confirmed. The main wheels were not locked and they collapsed on the landing roll. The aeroplane was landed without incident with only minor scuffing of fiberglass evident on rear of floats.
Outcome: It was identified that one of the air fittings was found with a small crack. It seems that this could have been there since installation and overtime with fair wear and tear has caused the fitting to fail. Fitting replaced and system tested with no further issues. |
28/11/2017 |
OCC1216 |
Moorabbin Airport |
VIC |
The Airplane Factory |
Sling 2 |
Rotax |
912 ULS |
During flight training the instructor demonstrated a glide approach, the student then practiced a gl...
|
During flight training the instructor demonstrated a glide approach, the student then practiced a glide approach which landed without incident. A second glide approach was initiated by the instructor and acted out by the student. The approach path was steady however speed was a constant 10kts higher than glide speed throughout most of the approach. Upon landing the student bounced and attempted to push the nose down, initiated a second bounce. This caused the student to push the nose down again which damaged the nose wheel upon impact. At this point the instructor took over and initiated a go around.
Another aircraft called in on Tooradin CTAF after witnessing the event and called stating that he suspects some nose wheel damage. The instructor asked the other aircraft if there were pieces of the aircraft on the runway to which he responds negative. The instructor elected to fly back to Moorabbin Airport at this point. The student flew the route back however the instructor made the approach and landing onto RWY 17R.
The landing was standard however, the nose wheel collapsed on the tarmac and the prop struck the ground. Once the aircraft came to a complete stop, the instructor notified ATC and shut down the fuel selector, magnetos and masters switch. Both the instructor and student sustained no injuries.
DETERMINED OUTCOME: Actions were taken by school CFI to temporarily ground the instructor following an accident debrief. Hand over take over procedures were reviewed, also a PMI review was completed to include landing upset strategies in the pre lesson brief. CFI advised fatigue may have also been a factor but the school adheres to CASA fatigue management guidelines. Also discussed emergency decision assessment and identification of damage in regard to declared emergencies. CFI conducted a successful instructor flight assessment in December and this was reviewed and debriefed with RAAus Operations . |
26/11/2017 |
OCC1219 |
Hamilton Island |
QLD |
ICP |
Savannah S |
Rotax |
912 ULS |
Upon arriving at Hamilton Island, with prior permission, the pilot was marshalled to the parking are...
|
Upon arriving at Hamilton Island, with prior permission, the pilot was marshalled to the parking area assigned to them. The aircraft was parked into wind and the wheels chocked, however there were no tie down facilities available. The pilot ensured the aircraft was secure and had no chance of moving before leaving the aircraft. Approx. 35m in front of the Savannah was a Beechcraft Baron also parked into wind. Around an hour later the pilot received a phone call advising that there had been an incident. Upon returning to the airport the pilot found that the Barron had been started without realising that the Savannah was parked behind them. The Baron had conducted engine & brake checks and consequently blasted the Savannah with the prop wash resulting in the Savannah being forced out of the wheel chocks and into the fence behind.
DETERMINED OUTCOME: No action required by RAAus. Captured for statistical reporting and data analysis. |
26/11/2017 |
OCC1222 |
Monarto |
SA |
Skyfox |
Ca21 |
Aero power |
2170 |
After take-off the aircraft was on a climb to 2500ft heading almost due south. At approx. 1500ft the...
|
After take-off the aircraft was on a climb to 2500ft heading almost due south. At approx. 1500ft the engine suddenly ran extremely rough. The pilot turned off the magnetos and the prop stopped in a vertical position. The pilot selected a paddock for an emergency landing. The pilot rounded out to select a high slow three-point landing and landed very heavily. The vertical propeller dug into the very soft ground causing the aircraft to tip upside down. The pilot escaped with only a small injury to the head.
OUTCOME: RAAus Technical team is unable to determine the cause of this occurrence. |
25/11/2017 |
OCC1214 |
Private Airstrip, Burrier |
NSW |
Morgan |
Cheetah Sierra |
UL Power |
260is |
Whilst landing, the main wheels were on the ground and the nose-wheel dropping, a gust of wind cause...
|
Whilst landing, the main wheels were on the ground and the nose-wheel dropping, a gust of wind caused the aircraft to become airborne for a short distance and the aircraft bounced. The pilot applied full power to go-around but did not have energy to stay airborne. The nose-wheel failed as the aircraft landed heavily sliding off to the left side, hitting a fence (star picket) then spinning around damaging the right wing.
DETERMINED OUTCOME: Confirmed operations of aircraft were within prescribed test flight area requirements and pilot was fully compliant to undertake flight. The owner/pilot has provided a satisfactory self assessment of accident contributing factors and has engaged with Ray Tulhurst from Morgan Aeroworks for repair and modification work. |
25/11/2017 |
OCC1221 |
5NM WSW of RAAF Base, Gingin |
WA |
Jabuiru |
J160D |
Jabiru |
2200B |
Whilst cruising at 3500ft tracking 065 degrees magnetic from the coast, a Bell 412 was spotted overh...
|
Whilst cruising at 3500ft tracking 065 degrees magnetic from the coast, a Bell 412 was spotted overhead. A decent and left turn was carried out to maintain separation. The pilot of the Jabiru did not believe that they had lost separation however action needed to be taken to maintain it.
DETERMINED OUTCOME: No further action required by RAAus. Pilot took appropriate action and the report will contribute to ongoing data analysis. |
21/11/2017 |
OCC1211 |
Port Pirie |
SA |
Jabiru J160-C |
J2200B |
Jabiru |
J2200B |
The aircraft experienced a loss of power followed by a complete engine failure resulting in an uneve...
|
The aircraft experienced a loss of power followed by a complete engine failure resulting in an uneventful landing in a paddock.\
OUTCOME: Operations review confirmed both pilot and aircraft were compliant with RAAus requirements but noted that this was the third reported engine related occurrence for this aircraft. The Technical team have reviewed the maintenance log books and have not found anything out of the ordinary. The owner is encouraged to continue to monitor this issue and provide any updates to RAAus and the manufacturer as they become aware of anything more. |