| Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
| 28/11/2016 |
OCC0837 |
East Sale |
VIC |
Air Creation |
Tanarg |
Rotax |
912 |
During a short flight, whilst passing over 2875’ high terrain (at altitude of 3800 ft) the aircraft ...
|
| During a short flight, whilst passing over 2875’ high terrain (at altitude of 3800 ft) the aircraft encountered moderate turbulence. During the flight preparation ARFOR wind was predicted (270 degrees 20 kts) above 2000ft. The pilot had flown over this local terrain many times before in similar conditions (mostly when R358 was deactivated). The pilot instinctively climbed to an altitude beyond the rough air (temporarily oblivious to the Active Altitude Restriction) and in doing so, the 4000ft LL was infringed.
OUTCOME: While remaining OCTA, the pilot encountered moderate turbulence and without considering the CTA lower limit, climbed to move out of the turbulent layer, inadvertently infringing CTA. He noted for future flights he would conduct pre-flight planning to contact ATC for a clearance as he is CTA qualified. |
| 27/11/2016 |
OCC0840 |
Wangaratta Airport |
VIC |
Esqual |
Vm 1c |
Rotax |
912S |
The aircraft was departure normal with full throttle. After take off, at approximately 10 ft in the ...
|
| The aircraft was departure normal with full throttle. After take off, at approximately 10 ft in the air, the left wing dipped and the pilot was unable to correct the aircraft angle. The wing tip made contact with the ground. The aircraft lost a propeller blade and the left wheel collapsed. All electrics switched off and there was no evidence of a fire at this point. After the pilot checked the passenger was uninjured they both exited the aircraft. On exiting the aircraft a small amount of smoke was seen from the engine compartment. By the time the pilot and passenger had cleared the aircraft (approximately 20 m away) it had caught fire, destroying it.
OUTCOME: The pilot was operating from a shorter grass strip, with additional traffic, due to the fly in activity. The pilot may have applied sufficient inputs to cause the aircraft to lift off earlier than usual, resulting in a stall. Corrective actions were not sufficient to prevent the aircraft from impacting heavily on the left wing, which caused the left wheel to collapse. The pilot and passenger were able to exit the aircraft, which was subsequently destroyed by the post impact fire. |
| 27/11/2016 |
OCC0839 |
Boonah |
QLD |
Skyfox |
Skyfox Ca22 |
Rotax |
912 |
The pilot gave a 10 NM inbound call to Boonah, then called joining downwind RWY04. No other calls we...
|
| The pilot gave a 10 NM inbound call to Boonah, then called joining downwind RWY04. No other calls were heard in the reply. Whilst on downwind the pilot noticed a shadow on the ground and saw a gliding tug on the inside (of downwind) for RWY04. This is the first the pilot was aware of the tug.
OUTCOME: This incident involved a RAAus registered aircraft and a glider in which both parties were counselled by the local RAAus CFI in regard to the aircraft separation incident. RAAus Assistant Operations Manager discussed this with the RAAus pilot and discussed the procedures for the area. It appeared that both the RAAus aircraft and glider did not follow airfield procedures. Ongoing discussions are occurring regarding the correct operating procedures between both types of aircraft at the field and it has been recommended that a safety meeting be conducted to clarify rules and procedures so that all parties can operate in the area harmoniously and without further issues. |
| 27/11/2016 |
OCC0844 |
Truro (Private strip) |
SA |
Skyfox Aviation |
Gazelle Ca25n |
Rotax |
912 |
While conducting touch and goes the aircraft touched down and started to roll when the pilot noticed...
|
| While conducting touch and goes the aircraft touched down and started to roll when the pilot noticed the wind sock had changed, showing the wind to be gusting in an S W direction. The pilot decided they were too far down the RWY to take off again so attempted to slow the aircraft, throttle back and braking, however the tailwind was too strong. At the end of the RWY was a taxiway which the pilot attempted to turn on to but the wind pushed the rolling plane against a low cyclone sheep fence as the aircraft turned.
OUTCOME: Pilot was conducting several "touch and go's" on a private strip and did not notice the wind had changed into a quartering tailwind. The pilot attempted to stop the aircraft however over ran the strip and impacted with a fence. The pilot noted that he should have monitored the wind direction more closely during the landings. |
| 25/11/2016 |
OCC0856 |
Hedlow Aerodrome (Rockhampton) |
QLD |
Airborne Windsports |
Edge X 912 |
Rotax |
912 UL |
Fatal Accident involving RAAus member and passenger. RAAus accident consultants are assisting police...
|
| Fatal Accident involving RAAus member and passenger. RAAus accident consultants are assisting police in determining the causal factors that led to the accident. A special Enews was sent out to members to inform them of the events http://www.vision6.com.au/em/message/email/view.php?id=1255251&u=70000&k=qu2fC0KuNRfQjgBl3liwmAQCTj3AGLPT3BhimQnR4Xk
Update: During a routine flight training exercise in a weightshift aircraft it appears the CFI and student were involved in a loss of control event while on approach to the airport. While RAAus assisted police with the preliminary investigation, the Coroner elected to utilise a third party to create the final report and at the request of the family has not publicly released a final report. RAAus preliminary investigations revealed no airworthiness issues with the aircraft nor concerns about the compliance, competence and currency of the pilots aboard.
As a general safety statement pilots of weight shift aircraft can significantly reduce risk when operating these aircraft by ensuring forecast weather conditions for the expected duration of the flight are within their capabilities and they are familiar with the characteristics of the aircraft wing and performance.
RAAus continues to work collaboratively with other organisations to ensure training in weightshift aircraft is relative to the advances in weightshift aircraft design and performance.
RAAus also works collaboratively with the Australian Transportation and Safety Bureau and local municipalities to investigate recreational aviation related fatalities. In this particular instance the Coroners actions have excluded RAAus from carrying out this function. |
| 25/11/2016 |
OCC0933 |
Chinchilla |
QLD |
ICP |
Savannah S |
Rotax |
912 |
Due to bushfire smoke the pilot was unable to get visual land marks until virtually over the top of ...
|
| Due to bushfire smoke the pilot was unable to get visual land marks until virtually over the top of them, as a result map reading became virtually impossible. This coupled with the failure of a backup GPS plus an increase in the severity of the turbulence resulted in the pilot became uncertain of their position, therefore rather than letting the situation progress to a more dangerous situation and as the aircraft was transponder mode S equipped, requested assistance from Brisbane Centre and Radar Vector. The pilot was vectored to circuit area Chinchilla where the aircraft landed safely.
OUTCOME: This is a classic "Swiss cheese" scenario pilots should be aware of when managing flights in smoke affected areas. While the pilot noted he was only using GPS for assistance and all navigation was completed using basic navigation and dead reckoning practices, increased smoke in the area was a major factor for a potential flight into IMC conditions. The lessons here for all pilots is to consider smoke haze as a similar hazard to cloud when planning flights. The pilot completed appropriate actions and prevented the holes in the “Swiss cheese” from lining up by engaging the assistance of Airservices which resulted in a positive outcome. |
| 23/11/2016 |
OCC0835 |
Binalong |
NSW |
Skyfox Aviation |
Skyfox Ca22 |
Rotax |
912 |
Whilst taxiing the aircraft, on a paddock strip in relatively long grass, the tail wheel did not rel...
|
| Whilst taxiing the aircraft, on a paddock strip in relatively long grass, the tail wheel did not release when turning. Consequently the propeller impacted thistles damaging propeller tips. The pilot had walked the intended path for taxi and take off prior to taxiing.
OUTCOME: While taxiing in a friends paddock for departure, the tail wheel aircraft did not turn as expected, resulting in the propeller impacting thistles and damaging the tips of the blades. Pilot admitted his mistake and will ensure the paddock is slashed to ensure vegetation is cleared prior to future flights. |
| 18/11/2016 |
OCC0828 |
West Sale |
VIC |
Aeroprakt |
A22LS Foxbat |
Rotax |
912IS |
Aircraft was readied for flight with a thorough pre-flight conducted prior to starting up, aircraft ...
|
| Aircraft was readied for flight with a thorough pre-flight conducted prior to starting up, aircraft was started and pre-take off checks completed, oil temp was at 65 degrees on commencement of the take off roll. As the aircraft became airborne it began losing thrust and stalled from about, 5ft striking the tail wheel first destroying it. Power was then returning causing loss of direction control until the pilot closed the throttle whilst heading for a drainage ditch. The pilot braked heavily and a partial ground loop was initiated causing the left wing tip to scrape the ground, front nose wheel dropped in to a hole while turning just prior to stopping bending the nose gear leg. On inspection of the aircraft back in the hangar it was noted that the propeller, whilst rotating it by hand, was notchy indicating a possibly bearing failure/gearbox failure had occurred causing the initial loss of thrust on take-off (there was no propeller strike during the incident).
OUTCOME: Manufacturer provided an engine tear down card as no actual engine tear down report was completed. The engine tear down card states that no fault with the mechanical or electrical data was found during the inspection. The engine has been returned to the owner for installation. |
| 18/11/2016 |
OCC0838 |
Wagga Wagga |
NSW |
Tecnam |
Echo Super |
Rotax |
912 ULS |
After a normal take off, during the climb the propeller stopped or almost stopped sufficiently to se...
|
| After a normal take off, during the climb the propeller stopped or almost stopped sufficiently to see the prop blade. There ensued a very large vibration causing a shake in the plane. The vibration was severe and the plane began to lose height. A quick check was made by the pilot which confirmed that the oil pressure was bottom of the green and oil temperature was into the yellow. The pilot then reduced to about 2500 RPM, the vibration decreased and the pilot increased to 2800 RPM and pushed the nose down a bit at the same time. Once the pilot was sure the engine was operating normally they resumed the climb and continued to their destination. When the aircraft levelled out all the gauges were green.
OUTCOME: Technical Manager liaised with the LAME/ L2. After inspection of the aircraft it was determined that the initial issue related to gearbox which has been rectified with no other defects detected. No other issues have been identified. The aircraft engine is currently over TTIS and requires the engine to be overhauled. Members are reminded of the importance of completing scheduled maintenance and overhaul processes on time. |
| 18/11/2016 |
OCC0829 |
Portland Airport |
VIC |
Jabiru |
J160C |
Jabiru |
2200 |
The pilot had conducted three circuits. On the final leg of the circuit approach from base at 700 f...
|
| The pilot had conducted three circuits. On the final leg of the circuit approach from base at 700 ft maintaining at 60 to 65 kt. The aircraft ballooned after contact with the ground and struck hard on second contact. The heavy landing broke the front wheel spat, a part of which fell off aircraft onto the RWY. The pilot detected that the spat was damaged on return to hangar and contacted airport groundsman of the potential hazard on the RWY.
OUTCOME: Report has been reviewed by RAAus Operations. The pilot stated that they reduced power too fast in the flare and did not apply or maintain sufficient power during ballooning period maintain flight. |
| 18/11/2016 |
OCC0827 |
Tamworth Airport |
NSW |
Evektor |
SportStar |
Rotax |
912 ULS |
During circuit training the instructor intended to conduct EFATO training as a lead up to a pre-solo...
|
| During circuit training the instructor intended to conduct EFATO training as a lead up to a pre-solo check session. All five preceding 'touch and go's', including two glide approaches, were normal and of an increasingly proficient standard. The Instructors intention on the full stop was to vacate by the first taxiway to minimise time on the RWY to assist with traffic in the circuit. The aircraft overshot the first taxiway and was still carrying a little power as the aircraft overshot the second taxiway. The brakes began to fade to the point of having no brake. The aircraft was still rolling at the end of the runway which necessitated departing the runway to the left into long grass. The aircraft was recovered successfully to the runway under its own power.
OUTCOME: Instructor did not manage students final approach to ensure sufficient runway remained for landing. |
| 17/11/2016 |
OCC0834 |
The Oaks |
NSW |
Foxbat |
A22 |
Rotax |
912S |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Two cracks detected on both doubler plates on carry t...
|
| OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Two cracks detected on both doubler plates on carry through rear spar channel, 90 degree bracket riveted onto inside of fuselage to carry through spar channel. Left side has one defined crack and to its right a small less defined crack, on the right hand bracket there are two fine cracks in the same area. The airframe has 3600 hours and this aircraft has been used for training its whole life. Also this aircraft was involved in an accident in Port Macquarie where its left wing impacted the ground after the nose leg was damaged following a heavy landing.
OUTCOME: This aircraft has previously been involved in an accident. The Australian agent believes that this accident is the possible cause for the crack developing. A repair process and parts are being supplied by the factory and repaired by a maintainer. Technical Manager has reviewed this report which is the first of its kind in this type of aircraft model. |
| 16/11/2016 |
OCC0825 |
Orange Airport |
NSW |
Jabiru |
J160 |
Jabiru |
2200B |
During early circuit training, a student on their first landing after a couple of weeks break lost d...
|
| During early circuit training, a student on their first landing after a couple of weeks break lost directional control on landing roll due to the crosswind and rolled to runway edge striking a runway light.
OUTCOME: RAAus Operations have reviewed this report. The loss of directional control was due to the inexperience of the student pilot in crosswinds. The student is continuing training with CFI. |
| 14/11/2016 |
OCC0826 |
Lismore |
NSW |
Jabiru |
J230-D |
Jabiru |
3300A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The aircraft transceiver has started to randomly flip...
|
| OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The aircraft transceiver has started to randomly flip-flop the standby frequency with the active frequency for no apparent reason. This has occurred once or twice at any stage of flight.
OUTCOME: Member has contacted the manufacturer directly due to this aircraft being a LSA. RAAus have this as the first recorded defect on this aircraft type and will liaise with the manufacturer if more reports of this nature are received. |
| 13/11/2016 |
OCC0881 |
Woodstock Airstrip |
QLD |
Arion Aircraft |
Lightning LS1 |
Camit |
3300A |
After touchdown, during the rollout, the nose wheel collapsed which also caused the Emergency Locato...
|
| After touchdown, during the rollout, the nose wheel collapsed which also caused the Emergency Locator Beacon (ELT) to activate. AMSA was notified that this was a minor incident with no injuries reported.
OUTCOME: The PIC advised that the nose wheel hinge block is only 140 mm off the ground. On rough strips the available suspension is limited, causing excessive stress on the nose wheel hinge junction. This is believed to be the common contributing factor to both this and a previous accident for this aircraft with different PICs. The PIC advised that operationally the nose wheel was held off appropriately and was not a consideration in this accident. RAAus Technical Manager also reviewed the report and advises members that as an experimental aircraft its the responsibility for the builder/owner to review and/or make necessary changes to address a particular fault. This aircraft is also made under the LSA process and there have been no other reported failures similar to this incident and will therefore continue to monitor for further incidents of this nature. |