Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
1/7/2016 |
OCC0695 |
Ballarat Airport |
VIC |
Esqual |
VM-1c |
Rotax |
912 |
Structural modifications were carried out on the aircraft due to a manufacturing flaw (causing signi...
|
Structural modifications were carried out on the aircraft due to a manufacturing flaw (causing significant forward and aft movement of the wings when manipulated by hand). The maintainer arrived at Ballarat to inspect the aircraft and test fly it on behalf of the owner. A thorough pre-flight inspection was carried out, and static engine run ups and taxi tests were conducted over a period of 2 hours. All systems were working as normal and pilot/maintainer taxied to RWY23 to line up for a circuit. Full power was applied, the ground roll and lift off was normal. On downwind a strong smell of petrol was noticed, so the pilot opened the vent in the window and proceeded to turn base. When on base (with a lower nose attitude) the pilot noticed a significant amount of fuel building up at their feet, estimated to be about 10 L. The pilot immediately turned all electrical switches off and pointed the aircraft to the runway. When the pilot was satisfied they could glide in on RWY23 they shut the engine down, unlatched the canopy hatch, and made an uneventful landing.
OUTCOME: Cause of the fuel leak were the fuel vents (this aircraft is a amateur built). The fuel vents on the original Esqual design were located inside the cabin. During the structural modifications, new fuel vent lines were routed to a position under the outboard section of each wing. The new fuel vents were made out of soft PVC tubing cut at a 45 degree angle. This was to give the tanks a slight positive pressure in flight. The fuel vents inside the cabin were never removed or plugged. When the aircraft gained sufficient airspeed after take off, the fuel tanks were pressurised from the airflow coming into the new vents. This in turn caused fuel to flow out of the original vents in the cabin. Fuel continued to flow through the old vents until the airspeed dropped to a level where the pressure was not great enough to continue the flow of fuel into the cabin. |
29/6/2016 |
OCC0693 |
Caloundra |
QLD |
Tecnam |
P92 Echo |
Rotax |
912ULS |
On landing and taxing to an area where the instructor could safely get out of aircraft for the stude...
|
On landing and taxing to an area where the instructor could safely get out of aircraft for the student to continue solo, the instructor noticed fuel coming from the lower engine cowling. The student shut the aircraft down, the fuel was shut off and aircraft pushed away from fuel on tarmac. Upon investigation the aircraft fuel filter in the engine cowling area was found to be stripped of its internal thread and was leaking.
OUTCOME: Technical manager reviewed report and on contact with aircraft operator found that the filter has been replaced and the fuel line has been re-positioned and secured by an appropriate L2. Nil defects evident since. |
29/6/2016 |
OCC0883 |
Orange |
NSW |
Aeropakt |
AP22 Foxbat |
Rotax |
912 ULS |
A student was on a solo flight within the circuit. The instructor was maintaining a listening watch ...
|
A student was on a solo flight within the circuit. The instructor was maintaining a listening watch on the radio and had not heard any calls from inbound aircraft nor an aircraft on approach. As such the circuit check had continued on without any knowledge of the second aircraft having to manoeuvre to avoid separation.
OUTCOME: According to the ATSB report there was radio congestion, as such a call from the inbound aircraft may have been missed during a period of high radio congestion whilst the instructor was supervising the student on their solo check. It is recommended that pilots keep a high level of vigilance during initial turn onto base and final. |
28/6/2016 |
OCC0702 |
Barwon Heads Airport |
VIC |
Sirius |
TL-3000 Sirius |
Rotax |
912 ULS |
After landing on RWY 22 (a grass strip, with medium length grass) the pilot exited the RWY however d...
|
After landing on RWY 22 (a grass strip, with medium length grass) the pilot exited the RWY however didn’t see a shallow drain and subsequently hit the propeller (prop strike). The engine was at idle and the pilot was surprised by the very lightweight construction of blades. Long grass contributed to the event (unable to see the drain).
OUTCOME: Taxiing incident - no further action required. |
27/6/2016 |
OCC0692 |
TBA |
NSW |
Jabiru |
J230-D |
Jabiru |
3300A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Maintainer has advised owner that the engine is defec...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Maintainer has advised owner that the engine is defective and considered no longer airworthy. The engine has previously over heated and maintenance has not been able to assist in the issues. The engine has a total time of 250 hours. Engine heads are warped and loosening therefore needing adjusting every 25 hours. Owner has requested assistance from RAAus.
OUTCOME: Owner advised that another maintainer has reviewed the engine and identified that the defect related to an engine cooling issue. Aircraft defect has been rectified with a manufacturer modification. |
27/6/2016 |
OCC0698 |
Unknown |
NSW |
Jabiru |
J230-D |
Jabiru |
3300A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The aircraft owners’ mechanic has determined that the...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The aircraft owners’ mechanic has determined that the engine may no longer be airworthy. The engine had a history of overheating, now the heads are warped and loosening therefore needing adjusting every 25 hours.
OUTCOME: Technical Manager reviewed the report and spoke with current maintainer. Maintainer stated that the engine was originally LAME maintained however during that time the LAME did not address issues with the head. The new maintainer conducted an inspection and decided that the engine should be removed prior to failure - a loan engine (Jabiru 3300A) has been fitted. The maintainer has indicated that the engine appears to have been previously run hot which may be have been due to the operator flying the aircraft with a lean mixture. To date nil defects evident since the engine replacement. |
25/6/2016 |
OCC0687 |
Mildura Airport |
VIC |
Morgan |
Cheetah |
Jabiru |
2.2 |
Nose wheel collapsed after landing however not due to a hard landing. Whilst on roll through the wel...
|
Nose wheel collapsed after landing however not due to a hard landing. Whilst on roll through the weld has given way on the nose wheel assembly.
OUTCOME: This is a 19 registered amateur build aircraft. This aircraft type has a history of failure in the nose wheel design and material in which the manufacturer has addressed previously and offered upgradable parts. |
25/6/2016 |
OCC0688 |
Caboolture |
QLD |
Tecnam |
P2002 Sierra |
Rotax |
912ULS |
Aircraft departed Caboolture to the West climbing through 3000 for 4500 ft when a burning smell was ...
|
Aircraft departed Caboolture to the West climbing through 3000 for 4500 ft when a burning smell was detected and then smoke in the cockpit (which appeared to be coming from beneath the seats). The pilot immediately turned back to Caboolture and the smoke started to dissipate (all happening within 60-90 seconds). The pilot continued back from the West declaring an emergency on the CTAF, as an aircraft was on takeoff roll from RWY30 and the pilot wanted to join long downwind for RWY30 to land as soon as possible. The pilot requested that the aircraft extend his takeoff on the RWY30 centre until the aircraft was past on the downwind leg (which they did). By the time the aircraft entered the downwind leg the smoke had completely dissipated and landed without incident.
OUTCOME: Inspection of the aircraft found that the strobe light fuse had blown which led to the Strobe Controller Box, situated under the pilot's left-hand seat. Inspection of the grill over the cooling fan found black marks and smelt of burning. A new fuse was inserted, ignition key turned on and strobe switch turned on. The fan in Strobe Controller Box started humming and smoke started to exit from the cooling fan grill, confirming where the smoke came from. The fuse was disconnected and maintainer removed the Strobe Controller Box. |
22/6/2016 |
OCC0691 |
Latrobe Valley |
VIC |
Tecnam |
P92 Eaglet |
Rotax |
912ULS |
Flat tyre upon landing. The pilot allowed the aircraft to roll to a stop just off the runway.
OUTC...
|
Flat tyre upon landing. The pilot allowed the aircraft to roll to a stop just off the runway.
OUTCOME:The tyre was re-inflated to allow the aircraft to taxi to the apron. The tyre became deflated shortly after parking on apron. |
17/6/2016 |
OCC0679 |
Welcome Creek |
QLD |
Austflight ULA |
Drifter A-503 |
Rotax |
503 DCDI |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Cracked bracket on starboard, outer, forward brace br...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Cracked bracket on starboard, outer, forward brace bracket. Further investigation being conducted.
OUTCOME: Technical Manager spoke with the owner of this aircraft who has identified this crack in the associated part during the dismantling stage. For reference the crack that was identified was on the negative G side of the bracket. The bracket would have failed only if a catastrophic, unrecoverable manoeuvre was performed on the aircraft and from discussion with the owner it appears that this very small crack may have been there for an extended period of time. This aircraft is being rebuilt from the ground up. The crack that was found, in the corresponding parts, are no longer available and the RAAus Technical Manager has recommended that the MARAP process would assist in replacing these parts. |
17/6/2016 |
OCC0690 |
Torquay |
VIC |
Eastwood Aircraft |
Tyro |
Rotax |
337 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Two Aircraft Data Sheets (ADS) have been provided wit...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Two Aircraft Data Sheets (ADS) have been provided with the aircraft (one dated 1998 and the other dated 2016) showing different MTOWs. Reporter has stated that there are no details whatsoever which show how the approximate payload came to be different and requested RAAus investigate the appropriate MTOW for this aircraft type.
The Eastwood aircraft Tyro is an amateur built aircraft (as are all 95.10 aircraft) and as such there is no design standard.
In the case of amateur built aircraft, so long as the weight increase is within the limits of the applicable regulations (300 kg for 95.10), all that is required is a declaration from the builder confirming the new MTOW. The aircraft owner is the sole party responsible for the airworthiness of an aircraft registered with RAAus. Should there be any concerns regarding the airworthiness of an RAAus registered aircraft the responsibility lies with the owner to ensure the aircraft is fit for flight. |
17/6/2016 |
OCC0686 |
Noosa Heads |
QLD |
Sling |
2 |
Rotax |
912ULS |
Airspace Infringement. Aircraft entered controlled airspace due to encountering moderate turbulence....
|
Airspace Infringement. Aircraft entered controlled airspace due to encountering moderate turbulence. The pilot wanted to climb as soon a possible as their passenger was not used to the turbulence however they mistimed the climb and ended up in controlled airspace.
OUTCOME: Pilot failed to apply appropriate planning and visual identification of ground references in regards to situational awareness in CTR operations. Planning, visual fixing and situational awareness were reviewed with the pilot by Operations. |
14/6/2016 |
OCC0684 |
Maryborough/Bendigo |
VIC |
Jodel |
D-9 |
VW |
1600 |
Owner purchased aeroplane fitted with a VW engine which had been hangared for 7 years without any fl...
|
Owner purchased aeroplane fitted with a VW engine which had been hangared for 7 years without any flying. The aeroplane was serviced to flying condition by a L2. The owner/pilot collected the aeroplane at Lethbridge with conditions of 9 degrees Celsius and wind 16.5kts. After a half hour flight the engine ran very rough and visible ported black exhaust. Carburettor heating was applied for 30 seconds however had no effect so the pilot discounted carby ice and diverted to Maryborough where the aeroplane was hangared overnight by the resident LAME. The next morning (on inspection) it appeared that the air filter had begun to disintegrate and the LAME disassembled and cleaned the carburettor. Pilot was confident that the air filter had caused the problem. After a test flight overhead the field, which did not disclose any problem, the pilot departed for Echuca. About 30 minutes into the flight the same problem appeared once again. The pilot immediately commenced a climb at full power and the problem disappeared. Next morning, overhead Echuca, the pilot conducted a test and conclusively found that the problem was carby ice. On the application of carby heat it took 2 1/2 to 3 minutes to clear the ice. After this the pilot departed for Narrandera and successfully managed the ice enroute, carefully monitoring a small manifold pressure gauge, with no further problems.
OUTCOME: Reporter is an experience pilot and CFI. The carby icing issues were identified and rectified with the aid of a LAME/L2. Members are advised that additional care should be taken when purchasing aircraft, or transporting aircraft, without having a known history of maintenance and operation of the aircraft. |
12/6/2016 |
OCC0683 |
NE pastoral property private strip |
SA |
Canadian Light Aircraft Sales & Services |
Bush Caddy - R80 |
Subaru |
EA81 |
On climb-out a sharp (but not severe) vibration, not previously experienced, was felt. All engine op...
|
On climb-out a sharp (but not severe) vibration, not previously experienced, was felt. All engine operating conditions were normal. A close-in low level circuit was completed and an uneventful landing performed. By this time the vibration had increased in frequency.
OUTCOME: Investigation revealed cut damage to the front edge of the reduction drive belt, an adjacent area of the belt bulged outwards as if an object had been caught between the belt and the sprocket, and several teeth stripped from the drive belt. A subsequent tear-down of the re-drive unit also revealed minor damage to a sprocket tooth at the edge which corresponded to the cut edge of the belt. It is surmised that, during the take-off run, a sharp stone was lifted from the gravel runway surface by the propeller and lodged in the reduction drive. Despite frequent past use of gravel strips this had not been previously experienced with this aircraft. |
12/6/2016 |
OCC0700 |
Sunbury |
VIC |
Flight Design |
CTLS |
Rotax |
912 ULS |
An aircraft with no altitude squawk was observed to enter the ML CTR from the West. Numerous calls w...
|
An aircraft with no altitude squawk was observed to enter the ML CTR from the West. Numerous calls were made however unable to raise the pilot over comms. The aircraft conducted random orbits and appeared lost. Departures from ML RWY 27 were suspended with ANZ124 delayed for approximately 10 minutes and eventually departing on a visual right turn east of Sunbury Township. A phone call to the Melton aerodrome operator eventually resulted in the aircraft contacting ML CENTRE 135.7. The pilot was provided with help to find Melton aerodrome for a landing and was asked to call the shift manager when on the ground. The pilot confirmed that he was lost and was surprised to hear of the disruption that he had caused.
OUTCOME: Pilot did not maintain appropriate level of visual awareness of their position (relative to planned track) and did not apply standard dead-reckoning or lost procedures when he became unsure of his position. Contributing factors were due to the pilot incorrectly programming YMEL way-point into GPS and called a GA examiner for assistance to identify ALA and nearby feature which was misinterpreted by both parties. The pilot was requested to undertake a flight review in relation to navigation planning and in-flight management with an RAAus Pilot Examiner which was successful. |