Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
16/11/2016 |
OCC0825 |
Orange Airport |
NSW |
Jabiru |
J160 |
Jabiru |
2200B |
During early circuit training, a student on their first landing after a couple of weeks break lost d...
|
During early circuit training, a student on their first landing after a couple of weeks break lost directional control on landing roll due to the crosswind and rolled to runway edge striking a runway light.
OUTCOME: RAAus Operations have reviewed this report. The loss of directional control was due to the inexperience of the student pilot in crosswinds. The student is continuing training with CFI. |
14/11/2016 |
OCC0826 |
Lismore |
NSW |
Jabiru |
J230-D |
Jabiru |
3300A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The aircraft transceiver has started to randomly flip...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The aircraft transceiver has started to randomly flip-flop the standby frequency with the active frequency for no apparent reason. This has occurred once or twice at any stage of flight.
OUTCOME: Member has contacted the manufacturer directly due to this aircraft being a LSA. RAAus have this as the first recorded defect on this aircraft type and will liaise with the manufacturer if more reports of this nature are received. |
13/11/2016 |
OCC0881 |
Woodstock Airstrip |
QLD |
Arion Aircraft |
Lightning LS1 |
Camit |
3300A |
After touchdown, during the rollout, the nose wheel collapsed which also caused the Emergency Locato...
|
After touchdown, during the rollout, the nose wheel collapsed which also caused the Emergency Locator Beacon (ELT) to activate. AMSA was notified that this was a minor incident with no injuries reported.
OUTCOME: The PIC advised that the nose wheel hinge block is only 140 mm off the ground. On rough strips the available suspension is limited, causing excessive stress on the nose wheel hinge junction. This is believed to be the common contributing factor to both this and a previous accident for this aircraft with different PICs. The PIC advised that operationally the nose wheel was held off appropriately and was not a consideration in this accident. RAAus Technical Manager also reviewed the report and advises members that as an experimental aircraft its the responsibility for the builder/owner to review and/or make necessary changes to address a particular fault. This aircraft is also made under the LSA process and there have been no other reported failures similar to this incident and will therefore continue to monitor for further incidents of this nature. |
12/11/2016 |
OCC0818 |
Oxley Island |
NSW |
Drifter |
Maxair xp |
rotax |
503 |
The aircraft preformed a forced landing in paddock due to mechanical failure from a broken throttle ...
|
The aircraft preformed a forced landing in paddock due to mechanical failure from a broken throttle cable. Where the throttle cable passes through the floor there was a sharp angle in the cable, and the outer cable had a slight kink in it, which caused wear on the inner cable (causing it to break).
OUTCOME: RAAus Technical Manager has review the report and reminds members who are owners of 19 amateur built aircraft that they are also required to conduct pre-flight inspections and appropriate maintenance. |
12/11/2016 |
OCC0820 |
2km South of Miling |
WA |
Jabiru |
J170D |
Jabiru |
2200 |
A mechanical failure of the engine occurred during a cross country training flight, resulting in an ...
|
A mechanical failure of the engine occurred during a cross country training flight, resulting in an emergency landing in an outfield. The engine presented no signs of any issues and all temps and pressures were well within operating standards at the time of the engine failure.
OUTCOME: Engine appears to have No. 4 piston collapse with conrod or big end impacting crankcase internals. Engine will be sent to manufacturer (LSA) to conduct a strip down and the surviving pistons will be crack checked by Aerospace NDI company. LSA aircraft which comes under ATSM standard with CASA. |
12/11/2016 |
OCC0819 |
Between Caboolture airport and Bribie Island |
QLD |
Aeroprakt |
A32 Vixxen |
Rotax |
912 ULS |
After leveling out at 1500ft the aircraft hit a patch of light to moderate turbulence, the passenger...
|
After leveling out at 1500ft the aircraft hit a patch of light to moderate turbulence, the passenger side door flew open and then sprung back inside the cabin jamming in the door frame. Pilot has suggested that a probable causes was due to the door flexing in the turbulence which allowed the front of the door to open slightly into airstream with the precipitating wind force overpowering the door latch.
OUTCOME: RAAus Technical Manager has reviewed this report and liaised with the LSA Manufacturer who is addressing the problem and an additional type lock or bracket has been suggested. The LSA manufacturer will be notifying all affected owners. |
9/11/2016 |
OCC0812 |
Orange Airport |
NSW |
Jabiru |
160C |
Jabiru |
2200B |
Aircraft experiences a bird strike on landing with no damage to aircraft reported.
OUTCOME: This i...
|
Aircraft experiences a bird strike on landing with no damage to aircraft reported.
OUTCOME: This is the first report regarding a bird strike in this area. RAAus will continue to monitor any bird strikes reports for this area and ensure information in the ERSA for the local area advises appropriate information. |
9/11/2016 |
OCC0817 |
Echuca Airport |
VIC |
Jabiru |
J160c |
Jabiru |
2200B |
Conducting circuits on a sealed RWY. As the main gear came into contact with the RWY there was a jol...
|
Conducting circuits on a sealed RWY. As the main gear came into contact with the RWY there was a jolt felt through the rudder pedals. The aircraft was more than halfway down the RWY and the pilot pushed the throttle to full power and initiated a go around. After the aircraft lifted off the RWY the pilot realized there was no rudder control at all. The pilot then flew a low level circuit and landed the aircraft safely without further incident.
OUTCOME: On inspection it was found that the rudder cable had broken on the rearmost thread (which is used to adjust cable length) where the cable is attached to the rudder pedals. The Jabiru Service Bulletin and inspection had been carried out by L2 about 3 weeks prior to the incident with no defects evident at the time. Due to this aircraft being an LSA and coming under the ASTM standards, de-identified information has been forwarded to CASA for follow up with the required manufacturer. |
9/11/2016 |
OCC1030 |
Broken Hill Airport |
NSW |
Aeroprakt |
A32 |
Rotax |
912 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The Bowden cable used to operate the carburettor heat...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: The Bowden cable used to operate the carburettor heat on this aircraft has been configured so that when the control knob in the cockpit is pilled, the cable end at the carburettor extends. The change f direction in the cable's action is achieved by the single wire carburettor heater control cable having a 180 degree bend half way along its length. In the form of a tight 'U', and doubling back along itself for a couple of inches. The cable sleeve is in two separate parts so that the portion of the cable with the 'U' bend is exposed, and free to move outside the sleeve. On this particular aircraft the cable sleeves were not supported at the ends near the 'U' bend. This allowed the cable sleeves to move with the control cable and prevent the carburettor heater valve from operating correctly.
DETERMINED OUTCOME: This issue has been rectified and the Maintenance Manager has also notified the manufacturer of the issue. |
8/11/2016 |
OCC0822 |
Darwin |
NT |
Flysynthesis |
Storch S500 |
Rotax |
912 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Upon removing the top and bottom cowls it was noticed...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: DEFECT: Upon removing the top and bottom cowls it was noticed that the starboard muffler had come adrift from its mounting and was in fact inside the bottom cowl. Some minor chaffing had occurred.
OUTCOME: After discussions with the maintainer it appears that previous maintenance practices, in regard to correct parts not being used, has not been complied with. The L2 has identified this issue and sourced parts from local supplier. |
8/11/2016 |
OCC0814 |
Simpson Desert |
NT |
The Aircraft Factory |
Sling 2 |
Rotax |
912 IS |
Warp Drive Propellor hub failed in flight after 5-10 seconds of vibration. The pilot attempted to fi...
|
Warp Drive Propellor hub failed in flight after 5-10 seconds of vibration. The pilot attempted to find a motor setting with minimal vibration however the ensuing failure occurred very quickly. The engine was then shut down and a forced landing site ensured. A "MAYDAY" was called and EPIRB activated. The landing was conducted as slow as possible with motor off, the flaps fully down, and switches off. The canopy was open (it opened after the hub failure due to the vibration) and the pilot ensured the passenger was tightly secured. The aircraft was damaged on landing however no injuries were reported.
OUTCOME: Factory have issued a service bulletin for an inspection schedule on the Warp Drive Propeller Hub at each 100 hourly. The factory will also supply a letter of authorisation for the fitment of Australian made Bolly 3 blade ground adjustable propellers. Members are reminded to contact the appropriate Search and Rescue authorities to clarify a safe landing when calling a "MAYDAY" and activation of a EPIRB. |
7/11/2016 |
OCC0811 |
Cobbity |
NSW |
Jabiru |
J160C |
Jabiru |
2200B |
A precautionary landing was conducted after the pilot noted engine vibration in normal flight.
OUTC...
|
A precautionary landing was conducted after the pilot noted engine vibration in normal flight.
OUTCOME: Aircraft has been inspected and a section of the propeller spinner back plate become dislodged during flight which caused the vibration. |
7/11/2016 |
OCC0810 |
Mount Phillip Homestead Airstrip |
WA |
Aeroprakt |
A-22LS |
Rotax |
912ULS |
During take-off the pilot opened the throttle to get up to speed however the aircraft did not seem t...
|
During take-off the pilot opened the throttle to get up to speed however the aircraft did not seem to be performing, despite the gauges reading okay. The pilot decided to abort the take-off however was too late to pull up before the end of the RWY. The aircraft went through a ditch and several bushes, coming to a stop approximately 45m from the end of the RWY. After inspection it appeared that the handbrake of the aircraft may have been engaged.
OUTCOME: Investigations revealed the hand brake of the aircraft may still have been engaged reducing the performance of the aircraft. Pilots are reminded of the importance of using checklists to ensure the aircraft is configured correctly for the intended phase of flight, and early actions to reject take-off if reduced aircraft response is recognised. |
6/11/2016 |
OCC0900 |
Buckland |
TAS |
Jabiru |
J120C |
Jabiru |
2200 |
On approach to a one way private airfield, an unexpected tailwind was encountered. The pilot was add...
|
On approach to a one way private airfield, an unexpected tailwind was encountered. The pilot was additionally forced to hold off the touch-down due to noticing unexpected loose stones on the approach end of the paddock. The plane was landed normally on the remainder of the paddock however the grassed surface had a pronounced undulation which greatly reduced the braking effectiveness. The plane was almost brought to a stop however made contact with some bushes at the far end, resulting in one propeller blade being broken.
OUTCOME: On approach to a one way private airfield, an unexpected tailwind was encountered, and in an effort to avoid loose stones an extended float occurred. The aircraft landed normally on the remainder of the paddock, but the grassed surface had a pronounced undulation which greatly reduced the braking effectiveness. The aircraft was almost stopped when it made contact with bushes at the far end, resulting in one propeller blade being broken. Appropriate engine teardown and required maintenance was subsequently conducted. |
4/11/2016 |
OCC0813 |
Narrogin Airfield |
WA |
Jabiru |
J170 |
Jabiru |
2200 |
Tow plane attempted to land and was prevented by an aircraft occupying the runway.
OUTCOME: RAAus O...
|
Tow plane attempted to land and was prevented by an aircraft occupying the runway.
OUTCOME: RAAus Operations contacted the pilot of the aircraft and recommended a ground and flight review to provide assurance of understanding of operations with gliders. |