Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
24/7/2022 |
OCC2891 |
Gawler Aerodrome |
SA |
Jabiru |
J160-C |
Jabiru |
2200 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: RAAus received a report of a pilot landing an RAAus aircraft ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: RAAus received a report of a pilot landing an RAAus aircraft at an airport very close to last light. The airport was not equipped with runway lights and the pilot acknowledged they should have planned to depart earlier and account for forecast headwinds, which delayed their arrival. |
22/7/2022 |
OCC2888 |
Barkley Homestead area |
NT |
Jabiru |
SP470 |
Jabiru |
2200A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The Jabiru departed EmKayTee (YMKT) first light with full win...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The Jabiru departed EmKayTee (YMKT) first light with full wing tanks (135 litres) for a non-stop flight to Barkley Station (YBKS). A planned flight time of 5.7 hours. The pilot had been tracking fuel use via fuel flow meter ranging between 13.5 - 15 litres an hour which was as expected, however 27 miles on the 320 radial short of the destination at 2500’ the engine ran rough and caught again. The pilot immediately switched on the electric pump and focused on a landing area on the black soil before flying over a highly treed area that separated the aircraft from Barkley Station. The engine ran for another 10-15 seconds before winding back to 1250-1300 RPM at full throttle. The pilot had been monitoring the LED fuel lights for the last hour of flight as they were dropping into the red then back to one green bar continuously. The pilot noted the fuel indicators may be unreliable and prefer to use Fuel Flow versus take off fuel. The pilot declared a MAYDAY on area frequency and when they received no answer switched to 121.5 and retransmitted the MAYDAY. Response was heard from QANTAS international flight who contacted Brisbane on their behalf. After landing successfully on the desert floor QANTAS handed the pilot over to another aircraft. The pilot of that aircraft stayed in touch with the Jabiru and Brisbane Centre for around 5 minutes. After losing contact with that aircraft the pilot was still unsure if their position was fully known so they activated their beacon and waited for further contact to be made. They tried Brisbane Centre several times with no success and each time transmitted their position "in the blind". The pilot tried both area frequency and Brisbane Centre on the hour and half hour times to conserve battery life but received no answer. Approx. 3.5 hours on the ground they heard a helicopter in the distance and contacted it on area frequency to be notified they were coming to assist. R22 landed 5-6 minutes later and flew them to Barkley Homestead where they cancelled their SARWATCH by phone. They confirmed there was only 1 POB and the EPIRB was deactivated before they left the landing area.
Once on the ground it was immediately obvious that the fuel drain for the header tank had permitted fuel to leak as the last litre had drained onto the desert floor and the remaining fuel (approx. 40 litres over 5.7 hours) had drained away in flight. At no time did the pilot smell any fuel leak. When the fuel total seemed to be low they visually checked both wing drains and fuel filter clamps and no obvious leak, visual or using smell was present.
RAAus Summary: The pilot has managed this situation well, and should be applauded for both MAYDAY call and activation of EPIRB. RAAus encouraged the pilot to think about fatigue considerations for such a long flight. |
22/7/2022 |
OCC2884 |
Lake King |
VIC |
Aerochute Industries |
Dual |
Rotax |
503UL DCDI |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Engine warm up normal for Rotax 503. Dual ignition check ok f...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Engine warm up normal for Rotax 503. Dual ignition check ok for rev. drop. Normal take off. Approx. 100ft off ground when engine started to run rough and then failed completely. The pilot did not attempt a restart because of low height, instead they glided the Aerochute onto the edge of Lake King and landed in the water. No damage to aircraft and nil injury to pilot and no property damage. There were no passengers on board. Recovered aircraft and took it to certified Rotax mechanic same day. Engine checked for water damage and OK. Clean fuel provided and engine started and ran normally. Mechanic believes engine problem was due to contaminated fuel as no other reason for the engine stopping can be found. This was the first time in two months that the aircraft had been used. |
22/7/2022 |
OCC2912 |
Canberra Aerodrome |
ACT |
BRM Aero |
Bristell S-LSA |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Just after takeoff at ~1700ft AGL as the aircraft was on dow...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Just after takeoff at ~1700ft AGL as the aircraft was on downwind and just handed off to approach the Co2 alarm went off in the aircraft. The pilot elected to discontinue the flight and informed ATC of the issue and then made a quick return onto runway 12 at YSCB with no further issues. No fault was found, and subsequent maintenance inspection requested by the pilot. |
19/7/2022 |
OCC2882 |
Dubbo |
NSW |
American Legend |
AL3 |
Continental |
O-200D48 |
Rudder cable contacting fuel line after fuel line had been pushed downward beside rear seat. Fuel li...
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Rudder cable contacting fuel line after fuel line had been pushed downward beside rear seat. Fuel line had deep cut/rub mark in it. |
19/7/2022 |
OCC2954 |
Serpentine Aerodrome |
WA |
Fly Synthesis |
Storch HS |
Jabiru |
2200A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Engine stopped on take-off and the aircraft was landed back ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Engine stopped on take-off and the aircraft was landed back on the runway. Engine restarted and ran normally during taxi back to hangar. Full engine inspection by L2 found cracking of the fuel lines immediately before the firewall; and out of sight near the gascolator at the bottom of the firewall. The remainder of the fuel lines looked and felt fine. The fuel lines still had 18 months before mandatory replacement. It was decided to replace all fuel lines and rubbers with new; sourced from manufacturer. It was also decided to remove the carburettor for a detailed inspection. Preliminary reason for engine stoppage is air ingestion due fuel line deterioration leading to failure at full power. |
16/7/2022 |
OCC2878 |
Streaky Bay |
SA |
Jabiru |
J430 |
Camit |
3300 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot completed a touch and go landing, then climbed out ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot completed a touch and go landing, then climbed out to complete one more landing. The pilot advised they should have deployed full flap to ensure good visiblity of the Single Wire Earth Return (SWER), but misjudged this approach and the aircraft clipped the SWER, resulting in damage to the aircraft and minor injury to the pilot. |
15/7/2022 |
OCC2885 |
Caboolture |
QLD |
Fly Synthesis |
Texan 599 |
Rotax |
912 ULS |
The new Rotax supplied Oil Radiator p/n 886002 is 6mm taller than its original OEM part. In the Texa...
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The new Rotax supplied Oil Radiator p/n 886002 is 6mm taller than its original OEM part. In the Texan 550, the new larger oil radiator does not fit into the carbon fiber housing as per the IPC. Being LSA, a manufacturer approved alternative mounting arrangement has been sought to mount the new size cooler in a Texan. |
14/7/2022 |
OCC2872 |
Aldinga Aerodrome |
SA |
Aeronca |
7AC |
Continental |
C90-14F |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: When on final for runway 32, on a very short final the pilot ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: When on final for runway 32, on a very short final the pilot did not leave sufficient room to clear a tree. The right wing tip clipped a tree. The aircraft yawed 20 degrees to the right and landed on 36 instead. |
9/7/2022 |
OCC2917 |
Coolangatta Aerodrome |
NSW |
BRM Aero |
Bristell S-LSA |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot landed on runway 14 and vacated on taxiway B. On v...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The pilot landed on runway 14 and vacated on taxiway B. On vacating the aircraft crossed the holding point without a clearance.
The pilot was unaware they had taxiied across a holding point but was aware that taxiway B was a hotspot. They thought that they had stopped in the correct location to contact ground for taxi clearance and pulled the data log from the Garmin in the aircraft, which seemed to indicate that they had stopped a metre or so past the second line which they agree was not correct.
The pilot has undertaken further review of the location and taxiway marking to ensure correct understanding |
8/7/2022 |
OCC2868 |
Devonport Aerodrome |
TAS |
Aeroprakt |
A22LS Foxbat |
Rotax |
912ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After circuit training with student, clear of runways and tax...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: After circuit training with student, clear of runways and taxing to GA area the left main tyre went flat. |
8/7/2022 |
OCC2865 |
Lismore Aerodrome |
NSW |
Jabiru |
J160C |
|
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: After conducting a crosswind landing during a period of dual ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: After conducting a crosswind landing during a period of dual training, another aircraft was sighted off the right hand side of the runway in grass (within the runway gable markers). The aircraft was passed without incident and the runway vacated to await the departure of the aircraft. The new CTAF frequency (132.45) had been monitored throughout the flight and regular base calls made by the training aircraft. No transmissions (e.g. taxiing or entering & backtracking) had been heard from the other aircraft, and the aircraft was not sighted by the student or instructor during the final approach until after touchdown. No damage or injury resulted from this incident. |
7/7/2022 |
OCC2864 |
Sunshine Coast Aerodrome |
QLD |
Sling |
Sling 2 |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Pilot certificate holder left pitot cover on. On takeoff, as ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Pilot certificate holder left pitot cover on. On takeoff, as rolling down runway, observed airspeed not climbing. Aborted takeoff and returned to hangar and did not fly.
RAAus noted the pilot had not flown solo for over a year.
It is recommended after any break in flying that pilots consider a refresher or review with an instructor, particularly in a new aircraft type. Pilots are recommended to review RAAP 1 Type Training and RAAP 5 What to expect from a BFR for more guidance. |
2/7/2022 |
OCC2861 |
Devonport Aerodrome |
TAS |
Tecnam |
P92 Echo Classic |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Local cross country flight was conducted with no issues. On l...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Local cross country flight was conducted with no issues. On late downwind approaching base power was eased back to idle for a glide approach when the pilot experienced some roughness in engine. Pilot checked to ensure the choke was not partially on and added slight power which momentarily seemed to ease rough running before experiencing a total engine failure. The pilot immediately turned toward the runway & transmitted a MAYDAY call on CTAF. Once final was safely established a restart procedure was commenced, the engine started and the aircraft was safely landed without incident.
Maintenance review has been conducted by a qualified maintainer who inspected carburettor bowls, needles and floats. Not issues identified and unable to replicate issue. Further checks for fuel pressure to be conducted. Further review ongoing, however, no fault has been able to be identified to date.
Determined Outcome: The aircraft owner reviewed the Carburettor Icing chart which stated that icing conditions were not present. Maintainer inspected the aircraft for defects with nil identified at time of inspection. The issue could not be replicated and has not occurred again in the seven months since the initial report was lodged. |
1/7/2022 |
OCC3121 |
Caboolture |
QLD |
Fly Synthesis |
Texan 599 |
Rotax |
912 ULS |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Defect: An earlier OMS reported that Rotax 912 ULS Oil Radia...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Defect: An earlier OMS reported that Rotax 912 ULS Oil Radiator Part No. 886002 was different in design to the original factory supplied component. An LOA was obtained by the aircraft manufacturer to allow changes to be made with regards to the fitting of the new size oil radiator to the aircraft. Rotax were contacted directly.
The original oil radiator was in excess of 10 years old, and whilst it showed no visible damage or wear, the decision was taken to replace the radiator due to higher than normal engine oil temps. Replacing the oil radiator after 10 years appears to have made a significant improvement to the engine oil running temperature. |