Date |
Occurrence # |
Location |
State |
Aircraft |
Model |
Engine |
Model |
Summary |
17/9/2021 |
OCC2547 |
Lake Samsonvale |
QLD |
Jabiru |
J160-C |
Jabiru |
Gen4 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The flight was from the Wivenhoe Dam Wall tracking for Redcli...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The flight was from the Wivenhoe Dam Wall tracking for Redcliffe, the pilot had previously requested clearance from Brisbane ATC to clear terrain but were refused even though CTA traffic was minimal.
The aircraft was at 2700ft on descent to 2500ft west of Lake Samsonvale aiming to be at 2500ft by the highway just west of the ATC boundary, when ATC informed them they had violated CTR. At no time did the pilot believe that they had penetrated CTR. At this time, a transponder code was provided and the flight continued to Redcliffe and onwards to Caloundra OCTA.
Upon landing at Caloundra the pilot was contacted by Australian Search and Rescue as they had not cancelled SARWATCH or Flight Following. At no time did the pilot request a SAR or Flight Following and ATC did not advise them that this had been implemented.
No corroborating report was provided from Airservices, no further action was taken. |
12/9/2021 |
OCC2529 |
Ballina |
NSW |
Jabiru |
J170 |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: It was reported that the aircraft had radio issues so the pi...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: It was reported that the aircraft had radio issues so the pilot returned to Lismore.
On inspection it was found that there was a broken wire in the pilots PTT switch under the control grip. A new PTT wiring harness was fitted. |
4/9/2021 |
OCC2523 |
Renmark Aerodrome |
SA |
Jabiru |
J160 |
Jabiru |
22B-192 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: On a flight from Callington to Renmark, and approx. 2-3 Miles...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: On a flight from Callington to Renmark, and approx. 2-3 Miles from Renmark the pilot of the RAAus aircraft called their approach from South East, descending from 3500ft. Approx. 30 to 60 secs later they observed a Glasair aircraft to starboard, approx. 200-300 metres horizontally and at their level, on climb, heading toward them. The pilot estimated the other aircraft would have cleared above them by 200 to 300ft
Both aircraft saw each other at the same time and veered to avoid conflict. The pilots communicated via radio and it is believed a miscommunication about the inbound aircraft may have resulted in the proximity event. |
2/9/2021 |
OCC2518 |
Flinders Is. |
TAS |
Jabiru |
Jabiru UL-T |
Jabiru |
2200 Gen 2 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: At approx. 800' ASL inbound to Lady Barron and about to make ...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: At approx. 800' ASL inbound to Lady Barron and about to make an inbound traffic broadcast the aircraft's engine started running very rough, then after about 30 seconds stopped completely. The pilot made a Mayday call on the Flinders Is. CTAF, then selected the nearest suitable clearing in the Tea tree scrub below and executed a forced landing without further incident. After exiting the aircraft, the pilot noticed that the aircraft's propeller was missing and that the propeller mounting bolts had all been sheared off. |
28/8/2021 |
OCC2514 |
Thargomindah |
QLD |
Jabiru |
SP470 |
Jabiru |
2200A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: On the take-off roll, on a solid sandy loam strip, the airc...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: On the take-off roll, on a solid sandy loam strip, the aircraft lurched left when the nose left the ground. Full right rudder was applied and as the edge of the runway approached (where there was a rill of dirt) the aircraft was coaxed off the ground in ground effect, straightened and manoeuvred back to the runway, where the aircraft touched both main wheels on the ground at an angle for a short period and then lifted off. Control was secured flying straight and level while the aircraft accelerated and then climbed out. At about 300ft AGL a dull thump started, and was later later determined to be the right hand landing gear which had broken away approx. 20cm above the lower bend and was being held in the air by the brake line.
A steady climb was achieved and flight at about 70kt was suitable to stop the thumping and all control surfaces were working well. A friend on the ground was contacted and was asked check the aircraft as it flew overhead. It was suspected that there may have been an undercarriage issue and this was confirmed.
The emergency services had been contacted and were on their way to the airfield. While waiting for the emergency services to arrive at the airfield, the aircraft climbed to 3000 ft AMSL and practiced stalls and then returned for a practice flyover so the ground crew could see what the issue was and land on the next time around on the dirt runway. The aux fuel pump had been running and the airspeed was about 65-70 kt. The aircraft was not able to gain height and the pilot was only doing gentle turns to (avoid a stall spin) due to concerns that the wheel could dislodge and hit a control surface. On the downwind leg abeam the threshold the engine stopped (possible carry icing). A glide speed of 60 kt was adopted and a gentle turn made towards the field. Fuel and all switches were shut off and the aircraft landed inside the fence in rocky but tree-free area. On impact the aircraft was doing about 35-40 kt and skidded to a stop with the tail raising to about a 50 degree angle off the ground then settled down. The pilot exited the aircraft. |
10/8/2021 |
OCC2505 |
Bundey Bore |
SA |
Jabiru |
J230 |
Jabiru |
J3300 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During landing on a gusty day, as the aircraft was about thre...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: During landing on a gusty day, as the aircraft was about three quarters of the way along the runway, a gust of wind picked up the right wing, the aircraft veered off into the scrub and the pilot was not successful in keeping the aircraft straight. The nose wheel made contact with a clumpy bush, caused the spat to jam the wheel and stop turning. The aircraft flipped vertically as a result and ended up on its back.
Once the aircraft was repaired the pilot completed a Biennial Flight Review with RAAus Flight Operations focusing on ensuring stabilised approaches and airspeeds and go-around assessments. |
27/7/2021 |
OCC2498 |
Mandurah Aerodrome |
WA |
Jabiru |
ST3 |
Jabiru |
2200J60 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was tied down at airfield when a severe storm o...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft was tied down at airfield when a severe storm overnight broke the tie downs and aircraft flipped upside down. |
24/7/2021 |
OCC2493 |
Tumby Bay Aerodrome |
SA |
Jabiru |
J230D |
Jabiru |
3300 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: A large weather event went through the Eyre Peninsula, the a...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: A large weather event went through the Eyre Peninsula, the aircraft had been repaired from the previous incident and waiting for the SA lockdown to end before it could be flown away. The aircraft was found upside down with the tie downs still attached to the aircraft, however they were pulled out of the ground. |
3/7/2021 |
OCC2468 |
Coffs Harbour Aerodrome |
NSW |
Jabiru |
J170-C |
Jabiru |
22B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a dual circuit lesson, after take-off at approx. 100 ...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: During a dual circuit lesson, after take-off at approx. 100 feet a small bird struck the aircraft on the spinner and inboard section of the propeller. The aircraft continued to operate normally and a standard circuit and landing was completed.
RAAus continues to monitor bird strike and wildlife reports at aerodromes to ensure correct ERSA/NOTAM information is in place. |
27/6/2021 |
OCC2465 |
Tumby Bay |
SA |
Jabiru |
230D |
Jabiru |
3300 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: During flight the pilot noticed a metal on metal burning sme...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: During flight the pilot noticed a metal on metal burning smell, they asked the passenger if they noticed it, they said it smelt electrical. At this point they were over water, within gliding distance of the land, so the pilot turned the aircraft toward the land. As they turned onto a westerly heading the aircraft lost both the Tacho & Oil Temp. there was a good oil Pressure reading but lost the temp. It was at the point the pilot chose to undertake a precautionary landing at Tumby bay. The aircraft was high at the current location so the pilot chose to do a descending turn and come out on final for runway 33 Tumby Bay. As the aircraft came over the threshold at about 20ft the pilot retarded power and begin to transition into a flare, as they did this about 20ft above the runway the engine totally ceased.
The investigation identified the flywheel bolts had failed. Repairs were undertaken and the aircraft was ready to fly, however a storm came through and flipped the aircraft upside down. As a result the aircraft was written off. Note: Jabiru Service Bulletin JSB012 refers to Jabiru Engine Flywheel Attachment |
24/6/2021 |
OCC2461 |
Lismore |
NSW |
Jabiru |
J170-C |
Jabiru |
2200B |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft experienced an engine failure and landed in a p...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft experienced an engine failure and landed in a paddock. |
13/6/2021 |
OCC2447 |
Chinchilla Aerodrome |
QLD |
Jabiru |
J160-C |
Jabiru |
2200 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The Jabiru was undertaking circuits at Chinchilla airdrome wi...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The Jabiru was undertaking circuits at Chinchilla airdrome with one other RAAus aircraft in the circuit. On late final on runway 14 just before touchdown the pilot of the other RAAus aircraft notified the Jabiru pilot that there was a third aircraft on late final for runway 32. The Jabiru pilot saw the other aircraft, just below the tree line at the opposite end of the airstrip, just as the call came through.
Both aircraft performed avoidance manoeuvres.
The Jabiru pilot changed frequency to 126.7 and contacted the third aircraft (VH registered) to inform them they were on the incorrect frequency and provided the correct frequency (126.35) to them. The pilot apologized and all continued flying. |
8/6/2021 |
OCC2435 |
Coffs Harbour Aerodrome |
NSW |
Jabiru |
J170-C |
Jabiru |
2200 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The student was conducting a session of solo circuits when Pi...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: The student was conducting a session of solo circuits when Pilot Induced Oscillation (PIO) occurred as a result of allowing the nose wheel to contact the ground too early. Lack of steering resulted in the aircraft running off the left hand side of the runway. No damage or injuries occurred and the student was able to taxi back onto the runway and return to the hanger. |
7/6/2021 |
OCC2436 |
Turkey Beach |
QLD |
Jabiru |
J230D |
Jabiru |
3300A |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: Sudden onset of severe engine vibration, reduced power to id...
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OCCURRENCE DETAILS SUBMITTED TO RAAUS: Sudden onset of severe engine vibration, reduced power to idle suspected possible propeller damage. Increased power but severe vibration still present and unable to maintain sufficient power for level flight. At an altitude of 3000ft the pilot selected a suitable landing area ahead, transmitted a mayday call on area frequency, and carried out an uneventful forced on a property west of Turkey Beach. On initial inspection there is no visible damage to propeller as first suspected. The engine cover was removed and there was no visible damage, however when turning the propeller, no compression was felt in engine, suspected internal engine damage. |
28/5/2021 |
OCC2431 |
Callington Aerodrome |
SA |
Jabiru |
J250 |
Jabiru |
A3300 |
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft experienced fuel starvation on take-off.
After...
|
OCCURRENCE DETAILS SUBMITTED TO RAAUS: The aircraft experienced fuel starvation on take-off.
After investigation it was found that the aircraft was actually flooding due to an incorrectly adjusted carby float. After resetting the float level and conducting full power ground runs the aircraft was successfully test flown. |